Aviation Accident Summaries

Aviation Accident Summary LAX95LA023

APPLE VALLEY, CA, USA

Aircraft #1

N5246G

GLEN A. SENECAL 5151

Analysis

THE PILOT LOST AILERON CONTROL WHILE PERFORMING A LOW-ALTITUDE FLYBY. THE PILOT LANDED THE AIRPLANE ON THE RUNWAY. THE REMAINING RUNWAY, HOWEVER, WAS INSUFFICIENT TO STOP THE AIRPLANE AND THE AIRPLANE EXITED THE RUNWAY. EXAMINATION OF THE AILERON REVEALED THAT THE AILERON CABLE SEPARATED FROM ITS ATTACH POINT. THE PILOT REPORTED THAT THE AILERON WAS NOT PROPERLY BALANCED.

Factual Information

On October 29, 1994, at 1208 hours Pacific daylight time, an amateur built Glen A. Senecal 5151 (a.k.a. midget mustang), N5246G, collided with the terrain after experiencing an aileron in-flight flutter at Apple Valley Airport, Apple Valley, California. The pilot was performing low flybys during an air show at Apple Valley Airport. The airplane, registered to and operated by the pilot, sustained substantial damage. The certificated private pilot, the sole occupant, was not injured. Visual meteorological conditions prevailed. The flight originated at Apple Valley Airport at 1153 hours. National Transportation Safety Board investigators conducted a telephone interview with the pilot on October 29, 1994. The pilot said that the airplane developed a severe aileron flutter condition when it was at midfield. The pilot immediately landed the airplane with its landing gears extended. The airplane touched down on the runway, but exited the runway environment during the skid. The main landing gear collapsed when the airplane entered onto the soft terrain. The pilot said in the aircraft accident report that the aileron was unbalanced. He said this condition caused the flutter. A Federal Aviation Administration (FAA) operations inspector from the Riverside [California] Flight Standards District Office witnessed the accident. He told Safety Board investigators that the flutter was very obvious from his vantage point. He said that he examined the airplane immediately after the accident. His examination disclosed that the right aileron cable was loose.

Probable Cause and Findings

the manufacturer's (owner/operator) improper balancing of the aileron flight controls which resulted in a cable separation due to overload from the aileron flutter. The rough/uneven terrain was also a factor.

 

Source: NTSB Aviation Accident Database

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