Aviation Accident Summaries

Aviation Accident Summary ATL95LA058

JEFFERSON, GA, USA

Aircraft #1

N1321Q

CESSNA 150L

Analysis

THE AIRCRAFT COLLIDED WITH TREES DURING AN EMERGENCY DESCENT. ACCORDING TO THE PILOT, DURING A NON-PRECISION, INSTRUMENT APPROACH, THE ENGINE BEGAN RUNNING ROUGHLY. CARBURETOR HEAT WAS APPLIED WITHOUT EFFECT, AND THE ENGINE QUIT. A RE-START WAS ACCOMPLISHED AND THE ENGINE RAN FOR A FEW SECONDS. IT BEGAN TO RUN ROUGHLY, AGAIN, AND QUIT. THE AIRPLANE COLLIDED WITH TREES AS THE PILOT ATTEMPTED TO REACH AN OPEN FIELD. THE PILOT/OWNER STATED THAT HE REGULARLY USED AUTOMOTIVE GASOLINE TO FUEL HIS AIRPLANE. THE USE OF AUTOMOTIVE GASOLINE IS NOT APPROVED BY THE MANUFACTURER OF THE ENGINE, AND CONTINUOUS USE OF AUTOMOTIVE GASOLINE MAY LEAD TO STICKING OR CORRODED ENGINE VALVES. AN EXAMINATION OF THE AIRCRAFT ENGINE REVEALED THAT THE LOSS OF POWER WAS CAUSED BY STUCK INTAKE AND EXHAUST VALVES WHILE IN FLIGHT.

Factual Information

On March 3, 1995, about 1735 eastern standard time, a Cessna 150L, N1321Q, collided with trees during an emergency descent. The pilot reported that there was a loss of engine power while conducting a non-precision, instrument approach into the Jackson County Airport, runway 34, Jefferson, Georgia. The airplane was operated by the pilot under the provisions of 14 CFR Part 91, and instrument flight rules (IFR). An IFR flight plan was filed for the personal flight. There were no injuries to the instrument rated private pilot, and the airplane was substantially damaged. Origination of the flight was Dayton, Ohio, about 1255, on the same day. According to the pilot, during the approach, the engine began running roughly. After passing the final approach fix, inbound, the engine RPMs dropped to 1400. Carburetor heat was applied without effect, and the engine quit. Atlanta Air Traffic Control Center records indicated, at 1735, the pilot notified air traffic control (ATC) that he had lost his engine. A re-start was accomplished, and the pilot notified ATC that he would complete the approach. The pilot stated that the engine ran at full power for a few seconds before it began running roughly, again, and quit. The pilot attempted a forced landing in a field 4 miles southwest of the airport. The airplane collided with trees approximately 50 yards before reaching the field. ATC notified local authorities that contact with the aircraft had been lost. Jefferson County Sheriff's Office personnel located the aircraft wreckage, and the pilot suffered no injuries. The pilot stated that he had last purchased fuel in Dayton, Ohio, where the aircraft was topped off with automotive gasoline. He also indicated that he regularly used automotive gasoline to fuel the airplane. According to the engine manufacturer, the use of automotive fuels in any of their aircraft engines is not recommended or authorized. Teledyne Continental Motors (TCM) authorizes only the use of fuels recommended in the engine operating manuals. The minimum fuel grade approved for use in the 0-200 model engine is 80 octane. According to TCM, all Continental aircraft engines are to be operated only on aviation fuel. The continuous use of automotive fuel can lead to sticking or corroded valves due to the absence of lead in the fuel. Lead is used to lubricate the valve in the valve guide in normal operation. Lead also cushions the valves as they are closed on the valve seat by the valve springs. Insufficient lubrication can lead to scuffing and scoring of engine valves. According to the pilot, he had experienced similar engine problems on a previous flight from Jackson County Airport, on February 26, 1995, to Dayton, Ohio. The pilot recalled that after climbing to 8200 feet, the engine began to loose power. The engine RPMs dropped from 2500 to 1500. The pilot applied carburetor heat, and the engine began to increase RPMs and run normal. The pilot stated that he believed he had corrected the problem, and that he was able to complete the remainder of the flight without any further problems. An examination of the engine showed evidence of severe scoring and scratching on all engine valves. The exhaust valves also showed coking on the stem that operated in the valve guide. The examination concluded that the loss of power was due to stuck valves while in flight. The Pilot/Operator Aircraft Accident Report, NTSB Form 6120.4, filled out by the pilot was never received. He declined to fill out a second report.

Probable Cause and Findings

THE LOSS OF ENGINE POWER BECAUSE OF STICKING VALVES. A FACTOR WAS THE CONTINUOUS USE OF AN IMPROPER FUEL GRADE.

 

Source: NTSB Aviation Accident Database

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