CHERAW, SC, USA
N3257W
SMITH MONNETT MONI
WITNESS REPORTS INDICATED THAT AFTER TAKEOFF, THE ENGINE BEGAN SPUTTERING. THE AIRPLANE WAS TURNED DOWNWIND TO RETURN TO THE RUNWAY. AS THE TURN TO THE BASE LEG WAS MADE, THE AIRPLANE STALLED AND PITCHED NOSE DOWN. IT IMPACTED IN A VERTICAL NOSE DOWN ATTITUDE. AN EXAMINATION OF THE ENGINE FOLLOWING THE ACCIDENT WAS INCONCLUSIVE. ANOTHER PILOT REPORTED THAT PRIOR TO THE ACCIDENT FLIGHT, HE AND THE PILOT DISCUSSED THE FUEL/OIL MIXTURE THAT WAS BEING USED FOR THE TWO CYCLE ENGINE. THE PILOT BELIEVED THAT THE FUEL MIXTURE HE WAS USING MAY HAVE BEEN TOO LEAN.
On June 21, 1995, at 1904 eastern daylight time, a George L.Smith Monnett Moni, N3257W, collided with trees and terrain following a reported loss of engine power near Cheraw, South Carolina. The private pilot was fatally injured, and the aircraft was destroyed. The homebuilt, experimental aircraft was operated under the provisions of 14 CFR Part 91 by the pilot. Visual meteorological conditions existed at the time, and no flight plan was filed for the local, personal flight. The flight originated at the Cheraw Municipal Airport, about 1904. A witness reported that the aircraft was on the downwind leg at the Cheraw Airport, and had been airborne about three minutes. She heard the engine sputtering prior to the crash. The airplane turned toward the airport and "nose dived." She said the engine was not running. Another witness was airborne, having departed prior to the accident pilot so they could fly together. He reported seeing the airplane enter an uncontrolled descent and impact the ground. A photograph of the wreckage, provided by the FAA inspector who visited the site, indicated aftward accordion-like damage from wing tip to wing tip. The nose of the airplane was crushed rearward, along the longitudinal axis of the fuselage. After the accident, the airborne witness stated that he and the pilot had a discussion, prior to the flight, regarding the fuel/oil mixture for the two cycle engine. The pilot had stated that he believed that he had been using a mixture that was too lean. A local mechanic inspected the airplane following the accident. He reported that the ignition system and flight controls checked satisfactorily. The spark plugs were clean. No fuel was discovered in the engine because the fuel tank had ruptured. He was unable to make any other determinations.
The loss of engine power for unknown reasons, and the pilot's failure to maintain flying speed, which resulted in impact with the ground while the airplane was in a stalled condition.
Source: NTSB Aviation Accident Database
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