Aviation Accident Summaries

Aviation Accident Summary FTW95LA374

COLORADO SPGS, CO, USA

Aircraft #1

N4814F

CESSNA 172N

Analysis

WITNESSES REPORTED THAT THE AIRPLANE DID NOT APPEAR TO BE CLIMBING NORMALLY AFTER TAKEOFF. THE PILOT RECALLED TURNING 'BACK TOWARDS THE RUNWAY.' THE PILOT-RATED PASSENGER RECALLED THERE HAD BEEN A POWER LOSS 'AS IF THE POWER HAD BEEN BROUGHT BACK TO IDLE.' SUBSEQUENTLY, THE LEFT WING DROPPED, AND THE AIRPLANE COLLIDED WITH TERRAIN. THE MIXTURE CONTROL WAS FOUND IN THE FULL RICH POSITION. A 4 INCH BY 3/8 INCH PIECE OF BAFFLE SEAL MATERIAL WAS FOUND NEXT TO THE VENTURI IN THE AIR INTAKE SIDE OF THE CARBURETOR THROAT, LODGED BETWEEN THE ACCELERATOR PUMP DISCHARGE TUBE AND THE POWER JET. THE UNDISTURBED CARBURETOR WAS FACTORY TESTED ON A SIMILAR ENGINE. THE ENGINE OPERATED 'EXTREMELY RICH.' ONE PILOT WHO HAD PREVIOUSLY FLOWN THE AIRPLANE SAID THE ENGINE DID NOT DEVELOP FULL POWER. ANOTHER PILOT-INSTRUCTOR SAID HE NOTICED THE ENGINE REQUIRED 'MORE LEANING' THAN OTHER CESSNA 172S HE HAD FLOWN. ELEVATION AT THE AIRPORT WAS 6172 FEET.

Factual Information

On September 1, 1995, at 0737 mountain daylight time, a Cessna 172N, N4814F, was destroyed when it collided with terrain after taking off from Colorado Springs, Colorado. The commercial pilot and passenger were seriously injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight being conducted under Title 14 CFR Part 91. The flight was originating when the accident occurred. In the Pilot/Operator Report, the pilot could not recall any of the accident details other than having initiated a left turn "back towards the runway." The pilot's father recalled that there had been a power loss, "as if the power had been brought back to idle." Control tower personnel observed the airplane take off on runway 35L, but it did not appear to be climbing. They asked the pilot if he was having difficulty or if he wanted to land. The pilot said he did not need any help. The left wing was then seen to drop and the airplane collided with terrain. The on-scene examination by a Federal Aviation Administration operations inspector disclosed the mixture control was in the "FULL RICH" position. A piece of baffle seal material, measuring approximately 4 inches by 3/8 inch was found lodged upstream from the venturi in the air intake side of the carburetor throat, between the accelerator pump discharge tube and the power jet. A similar piece of material was found missing from the carburetor heat air box. The elevation at Colorado Springs Municipal Airport is 6,172 feet above mean sea level (MSL). The undisturbed carburetor and carburetor heat air box were sent to Textron-Lycoming to be functionally tested. According to Textron-Lycoming's report, the baffle seal material obstructed air flow to the fuel discharge nozzle in the middle of the venturi. Although the accident engine was an O-320-H2AD, for test purposes the carburetor was mounted on a O-320-D3G engine. According to a Textron-Lycoming spokesman, there are internal differences between the two engines, but the test curves are the same. The engine was started and, according to one test engineer, operated "extremely rich." When the mixture was leaned, approximately 90 percent power (2,664 RPM) was attained. Full power (an air flow of 900 pounds per hour) could not be achieved due to the obstruction. Elevation at Williamsport, Pennsylvania, the test site, is approximately 529 feet MSL. A flight instructor, who was the last person to fly N4814F, said the airplane and engine operated normally for him on the day before the accident. The instructor, who owns a Cessna 172, said he had noticed that N4814F required "more leaning" than other Cessna 172s he has flown. One renter pilot, who had flown N4814F two weeks before the accident, stated that he made a night takeoff from Colorado Springs en route to Englewood, Colorado, and noticed the engine noise was "low" and the rate of climb was between 200 and 250 feet per minute (fpm). When he prepared to depart Englewood for the return trip, he performed an "extended" engine runup and made sure the mixture control was set properly and everything checked "normal." After takeoff and at an altitude of 15 to 20 feet above the ground, the airplane settled back towards the runway. The pilot was able to fly in ground effect until the airspeed increased. The airplane then climbed out at 100 fpm. He reported this to the operator the next morning, and the operator performed a cylinder compression check, finding nothing amiss, he returned the airplane to service.

Probable Cause and Findings

BLOCKAGE OF THE CARBURETOR BY A PIECE OF FOREIGN MATERIAL, WHICH RESULTED IN A LOSS OF ENGINE POWER, AND FAILURE OF THE PILOT TO MAINTAIN AIRSPEED, WHICH RESULTED IN AN INADVERTENT STALL. THE HIGH DENSITY ALTITUDE AND THE PILOT'S FAILURE TO PROPERLY LEAN THE FUEL MIXTURE WERE POSSIBLE FACTORS.

 

Source: NTSB Aviation Accident Database

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