Aviation Accident Summaries

Aviation Accident Summary LAX96LA099

OROVILLE, CA, USA

Aircraft #1

N992PK

Piper PA-28

Analysis

Seven minutes after takeoff, a total loss of engine power occurred, and the pilot made an emergency landing in a pasture. During the landing, the airplane collided with three fence posts and barbed wire. The pilot reported that he had not applied carburetor heat in response to the loss of power. Subsequent inspection of the aircraft revealed no mechanical malfunction, failure, or fuel contamination. After replacement of the damaged propeller, the engine was started and was operationally tested to 1500 rpm. The engine operated normally. About 31 miles south-southeast at Marysville, CA, the 2255 pst temperature and dew point were 55 and 41 degrees, respectively. According to icing probability charts, the reported temperature and dew point were conducive to moderate carburetor icing at cruise power.

Factual Information

On January 28, 1996, at 1537 hours Pacific standard time, a Piper PA-28-140, N992PK, experienced a loss of engine power in-flight and was substantially damaged in the ensuing off-airport emergency landing near Oroville, California. The private pilot was seriously injured. The flight had departed from Oroville about 1530 hours destined for nearby Paradise, California. Visual meteorological conditions prevailed and no flight plan was filed. The pilot told an FAA inspector from the Sacramento Flight Standards District Office that he was ferrying the aircraft to Paradise for its annual inspection, a distance of 13 miles. Soon after takeoff the engine lost power. The pilot identified an open field 7 miles northwest of Oroville for an emergency landing. During the landing the aircraft impacted three posts of a barbed wire fence, and then traveled an additional 100 yards before coming to rest with the nose wheel collapsed. The same FAA inspector examined the aircraft and reported that the annual inspection (license) on the aircraft had expired October 31, 1995. He also reported that the engine controls were intact and the fuel selector was on the right-hand fuel tank. The right-hand fuel tank was 3/4 full, and the left tank about 1/2 full. There was no contamination found in either fuel tank or the carburetor bowl. The carburetor heat box was damaged by impact and the control arm was pushed to the partial-on position by impact deformation of the structure. The inspector later ran the engine after a new propeller and temporary gravity fed fuel system was installed. The engine ran normally at 1,500 rpm with a magneto drop of about 90 rpm. The pilot told the NTSB investigator that he thought the engine failure may have been caused by carburetor ice, fuel contamination (water), or blockage of the fuel vent system by insects. He said that he did drain the fuel tank sumps before the flight and that he had not applied carburetor heat when the engine failed. An inspection of the fuel vent system by maintenance personnel did not reveal evidence of insect blockage. Forty minutes before the accident, at Marysville, California, the reported temperature was 55 degrees and the dew point 41 degrees. According to a carburetor icing probability chart, the reported temperature and dew point are in the area of the chart annotated as "moderate icing - cruise power."

Probable Cause and Findings

the failure of the pilot to use carburetor heat, which resulted in loss of engine power due to carburetor ice. The carburetor icing (weather) condition was a related factor.

 

Source: NTSB Aviation Accident Database

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