Aviation Accident Summaries

Aviation Accident Summary IAD96FA085

STEVENSVILLE, MD, USA

Aircraft #1

N103RW

Piper PA-31-310

Analysis

The pilot reported that he ran the engines to full power before releasing the brakes. Immediately after lift-off, when he retracted the landing gear, he noticed a dramatic loss of airspeed. The airplane began to rock back and forth, and the pilot's efforts to increase the airspeed including lowering the nose and adding full power was unsuccessful. According to the Piper Information Manual for a short field takeoff, a lift-off speed of 85 mph and 15 degree of flaps is required. The reported winds were 010 degrees at 7 knots. The pilot departed runway 29 which is 2910 feet long. A witness who was refueling an airplane on the ramp stated that the airplane was still on the runway at the 500 foot mark from the end of runway 29.

Factual Information

HISTORY OF FLIGHT On May 24, 1996, at 1055 eastern daylight time (EDT), N103RW, a Piper PA-31-310, lost engine power during initial climb from the Bay Bridge Airport and impacted the water in Stevensville, Maryland. The certificated private pilot, and the six passengers sustained minor injuries. The airplane was destroyed. Visual meteorological conditions prevailed and a flight plan was not filed. The personal flight was operated under 14 CFR Part 91. The flight originated at 1045 EDT and the intended destination was Laconia, New Hampshire. According to the pilot, he had completed a thorough preflight inspection of the airplane, which included draining the fuel tanks. He stated that a weight and balance within limits was accomplished also. He said the engine start and run-up check lists were completed uneventfully. The pilot stated that he applied the brakes, added full power and the airplane accelerated for takeoff. He said, "...I ran engines up to full power before releasing brakes at departure end of runway-all systems normal. Rotated at 105 mph. After gear up I noticed dramatic loss of airspeed. Plane began rocking from wingtip to wingtip-not sure it caused by power failure or turbulence. I pushed all controls forward-were all forward. Leveled pitch attitude of aircraft but airspeed loss continued. I was concerned that due to altitude and continuing loss of airspeed recovery would be impossible. My best and only option was to attempt a controlled landing in the water which I set up for and accomplished... ." A witness fueling an airplane on the ramp said, "...the Navajo went by me on the runway at approximately the 500 foot mark from the end of runway 29. It sounded as if the aircraft was not making full power and I went out to the edge of the runway to watch the aircraft depart the runway. When the aircraft became airborne it was not gaining altitude and leveled at approximately 75 to 100 feet off the runway. The aircraft landing gear retracted and the aircraft started to descend towards the water. The wings tipped from side to side indicating to me that the aircraft was just about at a stall. The wings never went more than approximately fifteen degrees to either the right or the left and the aircraft continued in a gradual descent... ." The aircraft was refueled on Wednesday, May 22 and had not flown since refueling. Fuel samples taken from the airport fuel sources after the accident did not disclose evidence of contamination. After the accident, the baggage was removed from the airplane and was not weighed. According to the Piper Information Manual the lift off speed and flap setting for a short field takeoff over a 50 foot obstacle is 85 mph and 15 degrees. The reported winds at the time of the accident was 010 degrees at 7 knots, and the runway is 2,910 feet long. Excerpts of performance chart, and airport information are appended. The airplane impacted water during the hours of daylight at 38 degrees, 58 minutes north latitude and 76 degrees, 20 minutes west longitude. PERSONNEL INFORMATION The pilot held a private pilot certificate with single and multi-engine land ratings. He also held an instrument airplane rating. According to the pilot operator report, he had over 2000 hours of total flight time including 600 hours in the accident make and model airplane. The pilot held a valid Federal Aviation Administration (FAA) third class medical certificate with no waivers/limitations, which was issued on March 20, 1996. AIRCRAFT INFORMATION The Piper PA-31-310 airplane, serial number 31-223, was equipped with two Lycoming TIO-540-A1B engines, left engine serial number L-543-61, and right engine serial number L-568-61. At the time of the accident, according to the pilot operator report, the pilot reported that the airplane had over 3812 hours of flight time. He stated that the most recent annual inspection was completed January 1996, and the airplane had accumulated over 101 hours of flight time since that inspection. METEOROLOGICAL INFORMATION At 1055 eastern daylight time, Baltimore Washington Airport, Baltimore, Maryland, located about 20 miles northeast of the accident site issued the following observation: Sky condition , 10,000 feet scattered; visibility 10 miles; temperature, 76 degrees Fahrenheit (F); dew point, 58 degrees F; winds out of 010 degrees at 7 knots; and altimeter, 30.01 inches Hg. WRECKAGE AND IMPACT INFORMATION An on-scene investigation was not conducted. The airframe and engine were examined at the Bay Bridge Airport, Stevensville, Maryland, on May 28, 1996. The parties to the investigation listed in this report participated in the examination. The airplane was retrieved from the Chesapeake Bay on May 27, and transported to the Bay Bridge Airport. The airplane was on the ramp with the gear in the down position. The fuselage was intact. The bottom of the fuselage was crushed. The right wing and aileron were damaged. The right wing had holes above the fuel tanks. The left wing was bent up at the midpoint. Flight control continuity was confirmed to the elevator, rudder and aileron from the cockpit. The elevator trim jack screw revealed four threads. According to a Piper representative this corresponds to a 9 degree tab down deflection. The flaps were found in the retracted position. The left engine was attached to the airframe. The left propeller remained attached to the engine. All three blades were bent back approximately 30 degrees at the midpoint. The engine did not rotate when turned manually. The oil suction screen was removed and there was evidence of water in the crankcase. The oil suction screen was clean. The right engine was attaced to the airframe. The right propeller remained attached to the engine. All three blades were bent back approximately 30 degrees at the midpoint. It was not possible to rotate the engine manually due to its location on the fuselage. The magnetos sustained water damage. The number 1 intake pipe was missing. The number 2 intake pipe was bent and detached. The exhaust and tail pipes below the turbocharger transition assembly were separated. The turbo bypass door assembly was damaged. The oil suction screen was removed and it was clean. It was determined that both engines and their accessories should be shipped to Lycoming's Reciprocating Engine Division, at Williamsport, Pennsylvania, for further examination. TESTS AND RESEARCH Further engine examination was conducted on July 19, 1996, under the supervision of the Federal Aviation Administration (FAA) from the Harrisburg, Pennsylvania, Flight Standards District Office. According to the Lycoming investigator, the examination of the left and right engine included removing the accessories and bottom spark plugs. All of the accessories were corroded and could not be tested. He reported that some of the spark plugs were oily, some contained debris and others exhibited moderate wear for both engines. The accessory housing was removed for the left and right engine. Engine internal timing was within limits for the left and right engine. Rotation of both engines was unsuccessful. The left engine cylinders were borescoped and removed. All the cylinders were corroded. Inspection of the cylinders and pistons revealed corrosion in the ring area of the pistons. When all the cylinders were removed the engine rotated. The turbocharger, controllers and the exhaust bypass valve were corroded. The turbocharger rotated freely. All cylinders on the right engine were sprayed with marvel mystery oil. After a few minutes the pistons freed and the engine rotated. Continuity was confirmed through the engine including the accessory drive train. All valves opened and closed. Compression was confirmed in all cylinders using the "Thumb Method." When boroscoped, all cylinder valves and piston domes were intact. The turbocharger compressor contained dirt and would not rotate. The compressor and turbine blades were intact. ADDITIONAL INFORMATION The airframe was released to the owner's insurance representative, Andy Paul, President, Crittenden Adjustment Company, Virginia Beach, Virginia, on June 4, 1996. The engines were returned to Executive Air in Hagerstown, Maryland.

Probable Cause and Findings

The pilot's improper short field takeoff/procedure and selection of the wrong runway for takeoff.

 

Source: NTSB Aviation Accident Database

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