Aviation Accident Summaries

Aviation Accident Summary SEA98LA029

EUGENE, OR, USA

Aircraft #1

N5190B

Cessna 152

Analysis

The pilot reported to the operator that the engine experienced a loss of power during the return leg of a cross-country flight. A forced landing was made on an open field. During the landing roll, the airplane collided with a fence. Inspection of the fuel tanks revealed that the left fuel tank was empty, and no fuel was produced when sumped. The right fuel tank contained approximately 1/8 of an inch of fuel, and produced approximately eight ounces of fuel when sumped. No fuel was added during the course of the cross-country flight.

Factual Information

On November 1, 1997, at 1833 Pacific standard time, a Cessna 152, N5190B, operated by Aerial Communications of America as a 14 CFR Part 91 personal flight, collided with a fence during a forced landing in a field located 14 miles northwest of Eugene, Oregon. Visual meteorological conditions prevailed at the time and no flight plan was filed. The aircraft was substantially damaged and the private pilot, the sole occupant, was not injured. The flight originated from Eugene at about 1400 and was destined for Elma, Washington. The flight was returning from Elma to Eugene, when the accident occurred. The pilot reported to the operator that the engine experienced a loss of power. A forced landing was made on an open field. During the landing roll, the airplane collided with a fence. Personnel from the airport, who helped recover the aircraft, reported that the tachometer indicated that 4.0 hours had been accumulated, and the Hobbs meter indicated that a total of 4.4 hours had been accumulated for the flight. The fuel tanks and sumps were inspected to determine the quantity of fuel remaining in the tanks. It was reported that there was no visible sign of fuel in the left fuel tank, and no fuel was produced when sumped. The right fuel tank contained approximately 1/8 of an inch of fuel, and produced approximately eight ounces of fuel when sumped. The engine sump produced approximately 14 ounces of fuel. Fueling records indicate that the aircraft was last fueled on October 31, 1997. The structural damage was not reported to the National Transportation Safety Board until January 27, 1998.

Probable Cause and Findings

the pilot's failure to refuel which subsequently led to fuel exhaustion.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports