Aviation Accident Summaries

Aviation Accident Summary SEA98LA125

PASCO, WA, USA

Aircraft #1

N4996X

Rockwell S-2R

Analysis

The pilot reported that while taking off to the west and climbing through about 40 feet above ground, the engine went to idle. He stated that he dropped his chemical load and immediately landed in an open potato field. The landing roll was crosswise to the furrows and the aircraft ultimately nosed over. FAA on-site inspection revealed a disconnect of the throttle linkage just forward of the firewall where it attaches to a 90 degree bell-crank designed to translate forward/aft motion into left/right lateral motion. The threads on the bell-crank attach end of the longitudinal throttle tube were found to be heavily worn.

Factual Information

On July 9, 1998, approximately 1000 Pacific daylight time, a Rockwell "Thrush" S-2R, N4996X, owned by Gerald Titus and being operated by Air-Trac, Inc., and being flown by a commercial pilot, sustained substantial damage when it nosed over during the landing roll following a near total loss of power on takeoff, seven nautical miles east-northeast of the Pasco airport, Pasco, Washington. The pilot was uninjured. Visual meteorological conditions existed and no flight plan had been filed. The flight, which was for the aerial dispensation of chemicals, was to have been operated under 14CFR137, and was departing from a private airstrip when it crashed. The pilot reported that while taking off to the west and climbing through about 40 feet above ground, the engine went to idle. He stated that he dropped his chemical load and immediately landed in an open potato field. The landing roll was reported to be crosswise to the furrows and the aircraft ultimately nosed over. FAA on-site inspection conducted by an inspector from the Spokane FSDO revealed a disconnect of the throttle linkage just forward of the firewall where it attaches to a 90 degree bell-crank designed to translate forward/aft motion into left/right lateral motion. The threads on the bell-crank attach end of the longitudinal throttle tube were found to be heavily worn.

Probable Cause and Findings

Separation of the throttle linkage which resulted in the loss of power. Factors include worn throttle linkage parts and the furrows in the plowed field which was the available field for the forced landing.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports