DETROIT, MI, USA
N452US
FOKKER F-28 MK 1000
THE CAPTAIN OBTAINED NO RESPONSE TO NOSE-UP STABILIZER TRIM DURING DESCENT. NORMAL NOSE-DOWN TRIM REMAINED OPERABLE; ALTERNATE TRIM WAS NOT ATTEMPTED. THE CREW REPORTED A JAMMED STABILIZER AND LANDED WITH NOSE-DOWN TRIM. DISASSEMBLY OF THE HORIZONTAL STABILIZER CONTROL UNIT SHOWED INADEQUATE LUBRICANT AND EXTENSIVE CORROSION IN A GEARBOX. THE AIRFRAME MANUFACTURER'S PROCEDURE FOR REPLENISHING THE GEARBOX LUBRICANT COULD RESULT IN UNDERSERVICING. THE OPERATOR OBSERVED A GEARBOX SERVICE INTERVAL WHICH WAS 250% OF THE MANUFACTURER'S RECOMMENDATION.
IMPROPER LUBRICATION OF THE HORIZONTAL STABILIZER GEARBOX BY COMPANY MAINTENANCE PERSONNEL. A FACTOR WAS THE MANUFACTURER'S INADEQUATE SERVICE PROCEDURE.
Source: NTSB Aviation Accident Database
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