Aviation Accident Summaries

Aviation Accident Summary ATL94LA020

MARYVILLE, TN, USA

Aircraft #1

N420FL

PIPER PA-28-140

Analysis

THE PRIVATE PILOT WAS FLYING FROM SANFORD, FL, TO KNOXVILLE, TN. DURING THE DESCENT INTO KNOXVILLE, THE ENGINE QUIT. HE SWITCHED TO THE LEFT TANK (THE RIGHT TANK INDICATED EMPTY) AND WAS UNABLE TO OBTAIN FULL POWER. THE ENGINE THEN QUIT AGAIN. WHEN HE ROCKED THE WINGS, THE ENGINE STARTED MOMENTARILY, THEN QUIT AGAIN. UNABLE TO MAINTAIN POWER ON THE ENGINE, HE FORCE LANDED THE AIRPLANE. THE WRECKAGE CAME TO REST ON POWER LINES NEXT TO A ROAD. THE LEFT WING WAS SEVERED FROM THE AIRCRAFT DURING IMPACT. PERSONNEL AT THE SITE FOUND NO EVIDENCE OF SPILLED FUEL. THE FUEL TANKS WERE RUPTURED AND FREE OF FUEL. THE PILOT REPORTED THAT HE TOOK OFF WITH 50 GALLONS OF FUEL, AND 6 GAL. WAS INDICATED IN THE LEFT TANK WHEN THE ENGINE QUIT. THE ACCIDENT FLIGHT DURATION WAS 5.7 HOURS. 75 PERCENT (CRUISE POWER) FUEL CONSUMPTION IS 8.4 GALLONS/HR.

Factual Information

On November 20, 1993, at 0124 eastern standard time, a Piper PA-28-140, N420FL, force landed following a reported engine power loss near Maryville, Tennessee. The private pilot was not injured. The aircraft was destroyed. The aircraft was operated by Aviation Training Associates of Sanford, Florida. The flight was conducted under 14 CFR Part 91. Night, visual meteorological conditions existed at the time, and a visual flight rules flight plan was filed for the personal flight to Knoxville, Tennessee. The flight originated in Sanford, Florida, at 1945 on November 19, 1993. The pilot reported the following: He was descending to land at McGhee-Tyson Airport in Knoxville when the engine quit. He had run extra long on the right fuel tank to keep the left tank as full as possible for landing. He switched to the left tank, but had trouble generating full power. The right tank fuel quantity gauge indicated zero gallons, and the left tank gauge indicated 6 gallons remaining. After rocking the wings, the engine started momentarily, then quit again. Unable to maintain engine power, he force landed the airplane about 3 miles to the east of the McGhee-Tyson Airport. The aircraft came to rest on the edge of a road, on top of downed power lines. The left wing was separated from, and adjacent to, the main wreckage. Personnel from the Blount County Fire Department reported that there was no evidence of spilled fuel at the accident site. A wrecker service operator recovered the wreckage shortly after the accident. He reported that the severed left wing was found about 10 feet from the main wreckage, and the fuel tank was ruptured. There was no fuel inside the tank, and no evidence of fuel spillage on the ground. The right wing was still attached to the fuselage. There was no evidence of fuel in the right fuel tank, and it was ruptured. There was no evidence of spilled fuel under the right wing. The wrecker service operator reported that he smelled no fuel fumes anywhere at the accident site. The pilot reported no mechanical problems with the aircraft. According to Federal Aviation Administration records, the aircraft was flown approximately 5.7 hours during the accident flight. The pilot reported that he began the flight with 50 gallons of fuel on board. According to the pilot's operating handbook for this aircraft, the fuel consumption at 75 percent (cruise power) is 8.4 gallons per hour.

Probable Cause and Findings

THE PILOT'S INADEQUATE INFLIGHT PLANNING, WHICH RESULTED IN FUEL EXHAUSTION PRIOR TO REACHING THE PLANNED DESTINATION.

 

Source: NTSB Aviation Accident Database

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