Aviation Accident Summaries

Aviation Accident Summary FTW92LA100

HAYDEN, CO, USA

Aircraft #1

N615AM

BOEING 757-223

Analysis

THE PILOT HAD REQUESTED THAT THE AIRPLANE BE PUSHEDBACK FROM THE TERMINAL APRON TO THE DE-ICING AREA PRIOR TO DEPARTURE. THE WEATHER WAS OVERCAST AND THERE WAS LIGHT PRECIPITATION WITH THE AMBIENT TEMPERATURE AROUND FREEZING. THE SIGNALMAN OPERATED THE HEADSET INTERPHONE WHICH WAS PLUGGED INTO THE COMMUNICATIONS PANEL ON THE NOSEGEAR STRUT. THE CREW CHIEF DIRECTED THE PUSHBACK FROM THE TRACTOR. THE SIGNALMAN WAS STRUCK BY THE NOSEWHEELS. ALL GROUND CREW PERSONNEL, EXCEPT THE SIGNALMAN, STATED THAT THEY HAD BEEN TRAINED BY VIDEO ON THE THREE MAN PUSHBACK PROCEDURES. THEY STATED, HOWEVER, THAT THEY DID NOT HAVE THE LONGER COMMUNICATIONS CORD AND THE CONNECTOR BOX ON THE TRACTOR, WHICH ARE NEEDED TO ACCOMPLISH THE PROCEDURES.

Probable Cause and Findings

FAILURE OF THE GROUND PERSONNEL TO FOLLOW PUBLISHED PROCEDURES/DIRECTIVES. A FACTOR WAS THE INADEQUATE EQUIPMENT.

 

Source: NTSB Aviation Accident Database

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