FAYETTE, MS, USA
N322A
BELL 47-D-1
PLT STATED THAT HE TOPPED THE FUEL TANKS TO THE 29 GALLON LEVEL PRIOR TO FLIGHT. ONE HOUR AFTER TAKEOFF THE ENG QUIT. HE STATED THE FUEL STRAINER DRAIN HAD LEAKED CAUSING FUEL EXHAUSTION AND LOSS OF POWER. TWO FAA INSPECTORS WHO INSPECTED THE ACFT AFTER THE ACCIDENT FOUND NO EVIDENCE OF PRE OR POST CRASH FUEL LEAKAGE. THE FUEL STRAINER DRAIN VALVE WAS FOUND TO OPERATE NORMALLY WITH NO EVIDENCE OF LEAKAGE.
THE PILOT IN COMMANDS FAILURE TO INSURE THE PROPER FUEL QUANTITY FOR THE FLIGHT WAS PLACED ON THE AIRCRAFT AND HIS FAILURE TO MONITOR FUEL QUANTITY DURING FLIGHT RESULTING IN FUEL EXHAUSTION.
Source: NTSB Aviation Accident Database
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