OLATHE, KS, USA
N9694K
STINSON 108-2
THE PILOT REPORTED A SEVERE SHUDDERING SHORTLY AFTER DEPARTING THE TRAFFIC PATTERN. POST ACCIDENT INSPECTION REVEALED THAT 7 INCHES OF ONE PROPELLER TIP HAD SEPARATED IN FLIGHT, CAUSING SEVERE IMBALANCE AND VIBRATION. THE PROPELLER TIP SEPARATED AT A REPAIR SCARF JOINT GLUE LINE.
THE IN FLIGHT SEPARATION OF THE PROPELLER TIP. AN ASSOCIATED FACTOR IS THE ROUGH AND UNEVEN TERRAIN.
Source: NTSB Aviation Accident Database
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