Aviation Accident Summaries

Aviation Accident Summary ANC92FA106

BETHEL, AK, USA

Aircraft #1

N20086

Short Brothers SC7

Analysis

THE AIRPLANE ROLLED 200-300 FT BEFORE BECOMING AIRBORNE IN A VERY NOSE HIGH ATTITUDE. IT MAINTAINED THIS ATTITUDE, MADE A RIGHT, THEN A LEFT BANK, AND FELL TO THE GROUND IN A NOSE HIGH ATTITUDE. THE CARGO CONSISTED OF EIGHT 55-GAL DRUMS OF FUEL, LAID ON THEIR SIDE AND SECURED BY ONE CARGO STRAP RUNNING FORE AND AFT AND ANOTHER CARGO STRAP RUNNING DIAGONALLY ACROSS THE BARRELS. THE TIE DOWN RING ULTIMATE STRENGTH RATING WAS 1600 POUNDS. THE WEIGHT OF THE CARGO WAS 2863 POUNDS. THREE OF THE CARGO HOOKS ASSOCIATED WITH THE CARGO STRAPS WERE FOUND STILL ATTACHED TO THE TIE DOWN RINGS, AND ONE HOOK AND TIE DOWN RING WERE NOT LOCATED. POST-IMPACT FIRE DESTROYED THE CARGO STRAPS, AND THE BARRELS WERE STREWN RANDOMLY THROUGH THE CABIN/CARGO AREA. ACCORDING TO THE MANUFACTURER, THE DAVIS TIE DOWN RING INSTALLATION IS NOT APPROVED BY THE MANUFACTURER. THE MODIFICATION SHOULD HAVE BEEN ACCOMPLISHED UNDER A SUPPLEMENTAL TYPE CERTIFICATE. THE LOGBOOKS SHOWED ONLY AN ENTRY. THE CERTIFICATED MAX GROSS WEIGHT WAS CALCULATED TO HAVE BEEN EXCEEDED BY 324.8 LBS.

Probable Cause and Findings

INADEQUATE SECURITY OF THE CARGO WHICH SHIFTED REARWARD DURING THE TAKEOFF ROLL. FACTORS WHICH CONTRIBUTED TO THE ACCIDENT WERE: THE OVER GROSS WEIGHT CONDITION, AND THE IMPROPER ALTERATION OF THE TIE DOWN RINGS BY THE OVERHAULING MAINTENANCE FACILITY.

 

Source: NTSB Aviation Accident Database

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