Aviation Accident Summaries

Aviation Accident Summary FTW93LA031

FORT STOCKTON, TX, USA

Aircraft #1

N925RR

CESSNA U206D

Analysis

THE AIRPLANE WAS IN CRUISE FLIGHT ON AN INSTRUMENT FLIGHT PLAN IN A LIGHT DRIZZLE AND ICING CONDITIONS WHEN A TOTAL LOSS OF POWER OCCURRED. THE PILOT ATTEMPTED TO RESTART THE ENGINE DURING THE FORCED LANDING. HE REMAINED IN COMMUNICATION WITH ATC DURING THE EMERGENCY DESCENT TOWARD THE CLOSEST AIRPORT. THE CONDITION OF LIGHT WAS DARK NIGHT AND THE PILOT REPORTED THAT HE DID NOT BREAK OUT OF THE WEATHER UNTIL NEARLY REACHING THE GROUND. THE LANDING AREA WAS ROUGH UNEVEN OPEN PRAIRIE. THE AIRPLANE WAS DAMAGED DURING THE LANDING. POST ACCIDENT EXAMINATION OF THE POWERPLANT REVEALED WATER IN THE FUEL SYSTEM IN THE DELIVERY LINE BETWEEN THE ENGINE DRIVEN FUEL PUMP TO THE FUEL CONTROL VALVE. ADDITIONALLY, WATER WAS FOUND IN THE INTAKE MANIFOLD. THE WATER WAS DRAINED AND THE ENGINE WAS TEST RUN WITHOUT INCIDENT. WHEN ASKED BY THE FAA, THE PILOT DID NOT KNOW ABOUT THE PUBLISHED FUEL TANK SUMPING PROCEDURE RELATIVE TO TRAPPED WATER IN THE BOTTOM OF THE CELLS.

Probable Cause and Findings

THE PILOT'S FAILURE TO FOLLOW PUBLISHED FUEL SYSTEM SUMPING PROCEDURES BEFORE FLIGHT AND TOTAL LOSS OF POWER DUE TO WATER CONTAMINATED FUEL. FACTORS WERE THE DRIZZLE AND ICING CONDITIONS AND THE LACK OF SUITABLE TERRAIN.

 

Source: NTSB Aviation Accident Database

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