ADVANCE, NC, USA
N74LE
BEECH V35B
THE PILOT REPORTED THAT DURING TAKEOFF THERE WAS A PARTIAL LOSS OF ENGINE POWER. HE WAS DISTRACTED WHILE TURNING ON THE FUEL BOOST PUMP. DURING THAT DISTRACTION THE AIRPLANE DRIFTED LEFT & COLLIDED WITH A BERM ADJACENT TO THE RUNWAY. HE STATED THAT THE ENGINE SURGED & WAS DEVELOPING FULL POWER WHEN THE COLLISION OCCURRED. SUBSEQUENT EXAMINATION OF THE ENGINE REVEALED ONE MAGNETO CONDENSER HAD MALFUNCTIONED WHICH RESULTED IN AN INCONSISTENT SPARK & SPUTTERING OF THE ENGINE.
THE PILOT'S DIVERTED ATTENTION AND FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE TAKEOFF. A FACTOR WAS THE MALFUNCTIONING MAGNETO WHICH RESULTED IN THE ENGINE SPUTTER.
Source: NTSB Aviation Accident Database
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