CHEHALIS, WA, USA
N6044P
PIPER PA-24-250
DURING A CROSS COUNTRY FLT, THE ENG LOST PWR. DURING THE EMERGENCY DESCENT, THE AIRPLANE COLLIDED WITH A BUILDING. THE POST CRASH ENG INSPECTION REVEALED THAT THE CRANKSHAFT GEAR WAS NOT SEATED PROPERLY DURING THE MAJOR OVERHAUL, WHICH RESULTED IN THE FATIGUE FAILURE OF THE CRANKSHAFT DOWEL. FURTHER RESEARCH REVEALED THAT DURING THE ENG OVERHAUL, A SERVICE BULLETIN WAS NOT COMPLIED WITH TO INSTALL A CRANKSHAFT GEAR THAT WAS MANUFACTURED WITH THREE, THREE QUARTOR INCH RADIUS SCALLOPS. THESE SCALLOPS ALLOW FOR INSPECTION OF THE GEAR AND CRANKSHAFT ASSEMBLY.
A LOSS OF ENGINE POWER DUE TO AN IMPROPER OVERHAUL.
Source: NTSB Aviation Accident Database
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