KINSTON, NC, USA
N311MC
BEECH 60
DURING TAKEOFF FROM RWY 22, THE PLT RPRTD THAT HE HAD A PROBLEM, THEN THERE WAS NO FURTHER COMM FROM THE ACFT. SVRL WITNESSES SAW AN OBJECT FALL FROM THE ACFT & ONE WITNESS OBSERVED THAT A 'HOOD' HAD OPENED. THE ACFT WAS MNVRD ONTO FINAL APCH TO RWY 36. A WITNESS SAID THAT AS THE ACFT WAS LINING UP ON FINAL APCH, IT ENTERED A STEEP BANK & DSCNDD OUT OF HIS SIGHT. SUBSEQUENTLY, IT COLLIDED WITH TREES IN A 27 DEG DSCNT, CRASHED & BURNED. A BAG FROM THE NOSE BAGGAGE COMPARTMENT WAS FND NEAR THE DEP END OF RWY 22. NO PREIMPACT PART FAILURE OR SYSTEM MALFUNCTION OF THE ACFT WAS FND. BEFORE THE FLT, A RAMP PERSON OBSERVED THE PLT SERVICING THE LEFT ENG WITH OIL, BUT HE DID NOT KNOW IF THE PLT HAD SECURED THE BAGGAGE DOOR. AN EXAM OF THE RCVRD DOOR ASSEMBLY FAILED TO DISCLOSE A MALFUNCTION OF THE REAR LATCH ASSEMBLY. THE FORWARD LATCH ASSEMBLY AREA WAS DESTROYED BY FIRE.
THE PILOT DIVERTED HIS ATTENTION AND FAILED TO MAINTAIN CONTROL OF THE AIRCRAFT, WHILE MANEUVERING FOR A PRECAUTIONARY LANDING. FACTORS RELATED TO THE ACCIDENT WERE: THE UNSECURED BAGGAGE COMPARTMENT DOOR AND THE PILOT'S INADEQUATE PREFLIGHT.
Source: NTSB Aviation Accident Database
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