FULLERTON, CA, USA
N2688S
CESSNA T-337-D
THE AIRCRAFT WAS ON A GO AROUND AT ABOUT 30 FT AGL WHEN THE FRONT ENGINE QUIT. THE PLT RETARDED BOTH THROTTLES AND LANDED; THE AIRCRAFT OVERRAN THE DEPARTURE END OF THE RUNWAY AND COLLIDED WITH A FENCE. THE FRONT ENGINE WAS OVERHAULED AND INSTALLED IN THE AIRCRAFT 2 HRS PRIOR TO THE ACCIDENT. EXAMINATION OF THE ENGINE REVEALED NUMEROUS DISCREPANCIES RELATING TO INCOMPLETE INSTALLATION OF THE ENGINE: TOOLS LEFT IN THE ENG COMPARTMENT; LOOSE AND NOT CONNECTED OIL AND FUEL LINES; IMPROPERLY CONNECTED THROTTLE AND MIXTURE CONTROLS; ETC. THE TURBO CONTROLLER WAS FOUND MISADJUSTED AND NOT PROPERLY CONTROLLING THE WASTE GATE VALVE. THE FUEL PRESSURE WAS SET EXCESSIVELY HIGH, WHICH CAUSED THE ENGINE TO QUIT WHEN RUN IN A TEST CELL. THE AIRCRAFT LOGBOOKS SHOWED THAT THE ENGINE INSTALLATION HAD BEEN SIGNED OFF BY AN AIRFRAME AND POWERPLANT MECHANIC AS COMPLETE.
THE LOSS OF POWER IN THE FRONT ENGINE DUE TO THE IMPROPER AND INCOMPLETE INSTALLATION OF THE ENGINE IN THE AIRCRAFT BY A MECHANIC.
Source: NTSB Aviation Accident Database
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