WINDSOR LOCKS, CT, USA
N425EX
BOEING 727-100QC
N425EX WAS ON THE TAKEOFF ROLL WHEN THE FLIGHTCREW EXPERIENCED A 'THUMP' THAT RESOUNDED THROUGH THE AIRPLANE. THEY ALSO OBSERVED ERRATIC ENGINE INDICATIONS FROM THE NO.3 ENGINE. THE CAPTAIN ABORTED THE TAKEOFF AND STOPPED THE AIRPLANE ON THE RUNWAY. THE FIRE WARNING SYSTEM ACTIVATED ON THE NO.3 ENGINE AFTER THE AIRPLANE CAME TO REST. THE CREW ATTEMPTED TO EXTINGUISH THE FIRE WITH THE AIRPLANE'S FIRE EXTINGUISHING SYSTEM; HOWEVER, THEY WERE UNSUCCESSFUL. THE POST ACCIDENT EXAMINATION OF THE NO.3 ENGINE REVEALED THE HIGH PRESSURE COMPRESSOR DISK HAD FAILED DUE TO A FATIGUE CRACK THAT ORIGINATED FROM A CORROSION PIT. THE SHRAPNEL FROM THE DISK PENETRATED THE ENGINE NACELLE AND SEVERED THE MAIN FUEL LINE FOR THE ENGINE. THE FUEL IGNITED AND BURNED INTO THE FUSELAGE, IGNITING THE 12,600 LBS OF CARGO (U.S. MAIL).
A CATASTROPHIC AND UNCONTAINED FAILURE OF THE NO.3 ENGINE WHICH RESULTED IN A FUEL FED FIRE.
Source: NTSB Aviation Accident Database
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