TWISP, WA, USA
N47KR
GREG SMITH KR-2
THE ENGINE QUIT WHILE THE PILOT WAS MANEUVERING AT A LOW ALT AGL AND THE ACFT IMPACTED TERRAIN DURING THE FORCED LANDING. INSP OF ACFT REVEALED A SHORTED MAGNETO CONDENSER WIRE. THE STU PILOT HAD NO INSTR ENDORSEMENT FOR THE FLIGHT OR LICENSE TO PERFORM MAINT INSP OF THE ACFT.
THE LOSS OF ENGINE POWER IN FLIGHT DUE TO SHORTED MAGNETO WIRES, RESULTING FROM INADEQUATE MAINTENANCE INSPECTION BY THE PILOT.
Source: NTSB Aviation Accident Database
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