VISALIA, CA, USA
N306AT
GLASAIR SH-2-RG
THE CERTIFICATED PRIVATE PILOT/OWNER STATED THAT AN HOUR AND HALF INTO THE FLIGHT THE ENGINE STARTED TO RUN ROUGH AND LOST RPM. ALL INSTRUMENTS WERE IN THE GREEN. HE HEADED THE AIRCRAFT FOR A SUITABLE AIRPORT BUT THE ENGINE QUIT IN THE PATTERN. DUE TO WINDS HE WAS UNABLE TO MAKE THE RUNWAY. EXAMINATION OF THE ENGINE BY FAA INSPECTORS REVEALED THAT THE NUMBER 4 CYLINDER EXHAUST VALVE FAILED.
TOTAL LOSS OF ENGINE POWER DUE TO THE FAILURE OF THE NUMBER 4 ENGINE EXHAUST VALVE.
Source: NTSB Aviation Accident Database
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