Aviation Accident Summaries

Aviation Accident Summary CHI91LA299

BOSCOBEL, WI, USA

Aircraft #1

N915PM

PIPER PA-23-250

Analysis

PURPOSE OF THE FLT WAS FOR THE PIC TO GET A MULTI-ENG (ADD-ON) RATING. DRG A 2 ENG GO-ARND, THE DESIGNATED PLT EXAMINER (DPE) SIMULATED AN ENG FAILURE BY RETARDING THE L THROTTLE. SOON THEREAFTER, THE AIRSPEED DECREASED & THE PIC ADZD THE DPE THAT HE WAS UNABLE TO MAINT ALT OR ATTITUDE. THE L THROTTLE WAS RE-ADVANCED WITH NO APPARENT EFFECT. THE PIC WAS UNABLE TO RESTORE PWR IN THE L ENG & RELINQUISHED THE FLT CTLS TO THE DPE. THE ACFT WAS PREPARED FOR AN APCH TO THE ARPT. WITH THE L ENG (& HYD SYS) INOP, THE PIC USED THE MANUAL HAND PUMP TO OPER THE GEAR & FLAPS (AFTER ASSURING THE ACFT WOULD CLR OBSTACLES). HE CONTD PUMPING, BUT THE ACFT WAS FORCED TO LND SHORT OF THE RWY & THE NOSE GEAR COLLAPSED DRG TCHDWN BFR IT WAS FULLY EXTDD. THE WING FLAPS WERE FND EXTDD. THE LNDG GEAR & WING FLAPS OPERD FM THE SAME HYD SYS; EITHER COULD HAVE BEEN ACTUATED INDEPENDENTLY OF THE OTR. THE HYD SYS WAS BUILT SO THAT WHEN THE GEAR & FLAPS WERE ENGAGED AT THE SAME TIME, THE GEAR WOULD COMPLETE ITS OPN BFR THE FLAPS OPERD. NO REASON FND FOR LOSS OF PWR IN L ENG.

Probable Cause and Findings

IMPROPER REMEDIAL ACTION BY THE PILOT-IN-COMMAND (PIC), AND INADEQUATE MONITORING BY THE DESIGNATED PILOT EXAMINER (DPE) DURING A SIMULATED EMERGENCY PROCEDURE. FACTORS RELATED TO THE ACCIDENT WERE: THE LOSS OF POWER IN ONE ENGINE DUE TO AN UNDETERMINED REASON, AND OBSTRUCTIONS IN THE EMERGENCY LANDING AREA THAT REQUIRED A DELAY OF GEAR EXTENSION IN ORDER TO REACH A CLEAR AREA.

 

Source: NTSB Aviation Accident Database

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