DFW INT'L ARPT, TX, USA
N425AE
BRITISH AEROSPACE BAE 3100
DURING THE TAKEOFF ROLL, THE PILOT OBSERVED THE TORQUE INDICATIONS OF THE RIGHT ENGINE DROP TO 80 PERCENT AND THE FIRE WARNING LIGHT FOR THE SAME ENGINE ILLUMINATE. THE PILOT ABORTED THE TAKEOFF AND DEPLANED THE PASSENGERS. AIRCRAFT FIRE AND RESCUE PERSONNEL EXTINGUISHED THE FIRE IN THE RIGHT ENGINE. A TEARDOWN AND ANALYSIS OF THE RIGHT ENGINE REVEALED THAT THE ELECTRICAL CONNECTOR OF THE TORQUE SENSING UNIT BECAME LOOSE. THE LOOSE CONNECTION RESULTED IN EXCESS FUEL BEING DUMPED IN THE ENGINE CAUSING A POOLING FIRE.
THE PARTIAL DISCONNECTION OF THE ELECTRICAL CONNECTOR AT THE TORQUE SENSING UNIT.
Source: NTSB Aviation Accident Database
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