BINGHAMPTON, NY, USA
N511AR
Cessna T303
While in cruise flight, at 6,000 feet, the left engine lost power. The pilot attempted a restart of the engine, but only about one-half rotation of the left engine propeller was observed, and the engine was secured. The pilot stated that he was unable to maintain altitude and initiated a decent. He requested and was cleared for an instrument approach at an airport where the weather conditions were, 1/4 statute mile of visibility, fog, and a vertical visibility of 100 feet. On the approach, at the minimum decent altitude, the pilot executed a missed approach. As the airplane climbed, the pilot reported to the controller that the 'best altitude [he] could get was 2,200 feet.' A second approach was initiated to the reciprocal runway. While on the second approach, the pilot 'was going to fly the aircraft right to the runway, and told the controller so.' He put the gear down, reduced power, and decided there was 'no hope for a go-around.' He then 'flew down past the decision height,' and about 70-80 feet above the ground, 'added a little power to smooth the landing.' The pilot also stated, 'The last thing I remember was the aircraft nose contacting the runway.' A passenger stated that once the pilot could not see the runway, [the pilot] 'applied power, pitched the nose up,' and attempted a 'go-around' similar to the one that was executed on the first approach. Disassembly of the left engine revealed that the crankshaft was fatigue fractured between connecting rod journal number 2 and main journal number 2. Review of the pilot's operating handbook revealed that the single engine service ceiling, at a weight of 4,800 pounds, was 11,700 feet. The average single engine rate of climb, at a pressure altitude of 6,000 feet, was 295 feet per minute. The average single engine rate of climb, at a pressure altitude of 1,625 feet, was 314 feet per minute. Review of the ILS approach plate for Runway 34 revealed that the decision height was 200 feet above the ground.
HISTORY OF FLIGHT On November 1, 1999, about 0616 Eastern Standard Time, a Cessna T303, N511AR, registered to Twin Cities Air Service Incorporated, was substantially damaged while landing at the Binghamton Regional/Edwin A. Link Airport, Binghamton (BGM), New York. The certificated commercial pilot received serious injuries and two passengers received minor injuries. Instrument meteorological conditions prevailed, and an instrument flight rules (IFR) flight plan was filed for the on-demand air taxi service, conducted under 14 CFR Part 135. According to the pilot, he conducted a preflight inspection of the airplane and added a quart of oil to each of the airplane's two engines prior to departing from the Auburn/Lewiston Airport, Auburn, Maine, at 0320. The pilot then flew the airplane to the Portland International Airport (PWM), Portland, Maine. The flight took about 12 minutes and was uneventful. At PWM, two passengers boarded the airplane, and the flight departed, destined for the Youngstown-Warren Regional Airport, Youngstown, Ohio. About 2 hours into the flight, at 6,000 feet, the left engine "suddenly stopped." The left engine oil pressure gauge fluctuated and then went to zero. The pilot observed the propeller to be "windmilling, but turning at a rate." After the left engine failed, the pilot placed the throttles, mixture, and prop controls for both engines in the full forward position to attempt a restart of the left engine, but since "we were in cruise mode, I did not immediately try to feather the engine, but tried the obvious restart procedures." During the attempted restart, the pilot observed only about one-half rotation of the left engine propeller. He also changed the position of the fuel selector to the left engine, but could not remember what position he finally selected. The boost pump switch was placed in the low position, and then into the high position. Both magnetos were shut off for the left engine, and the pilot attempted to feather the propeller. The attempt to feather the propeller failed. The pilot believed "the prop was turning slower than normal, [and] the locks may have come out, making it impossible to feather." The pilot did recall that the propelled eventually feathered later in the flight. The pilot added that during the processes of attempting to restart the engine, and then securing it, he noticed that the airplane's speed was "slowly bleeding down, to a point when it got to blueline." The pilot pitched the airplane down to maintain the blue line speed. Unable to maintain the airplane's altitude, the pilot initiated a decent. The airplane descended to 3,200 feet, described by the pilot as a "slow, gradual, sink." Once the left engine was secured, the pilot radioed to the Binghamton Approach controller that he "had an engine failure" and needed to land at the "closest VFR airport." According to the pilot, the controller replied that the closest VFR airport was 60 miles away. The pilot decided to land at BGM because it was nearby and he knew they had radar on the field. An instrument landing system (ILS) approach was conducted to Runway 16 at BGM. On final approach, the landing gear was not selected to the down position until the last minute so that the pilot would have the option of executing a go-around. Once he descended to his minimum decent altitude, the only visual contact the pilot had with the runway environment were 3 unidentified lights, and a missed approach was initiated. As the airplane climbed, the pilot reported to the controller that the "best altitude [he] could get was 2,200 feet." Since the approach called for a higher altitude, the controller "started" him in on an ILS approach to Runway 34 "inside the marker." The pilot added that, while on the second approach, "I was going to fly the aircraft right to the runway, and told the controller so." The pilot put the gear down, reduced power, and decided there was "no hope for a go-around." He then "flew down past the decision height," and about 70-80 feet above the ground, he "added a little power to smooth the landing." The pilot also stated, "The last thing I remember was the aircraft nose contacting the runway, I may have instinctively pushed the throttle forward..." A passenger stated that once the pilot could not see the runway, "he [the pilot] applied power, pitched the nose up," and attempted a "go-around" similar to the one that was executed on the first approach. The airplane's wing tip then hit the ground. The accident occurred during the hours of dawn approximately 42 degrees, 12 minutes north latitude, and 75 degrees, 58 minutes west longitude. PERSONNEL INFORMATION The pilot held a commercial pilot certificate with ratings for airplane single engine and multi-engine land, instrument airplane. He also held a flight instructor certificate for airplane single engine land, instrument airplane. The pilot's most recent Federal Aviation Administration (FAA) first class medical certificate was issued on January 18, 1999. The pilot reported approximately 2,430 hours of flight experience, 200 hours of which were in multi-engine airplanes, and 60 hours of which were in make and model airplane. The pilot reported 180 hours of flight experience in the 90 days prior to the accident. His most recent biennial flight review was August 27, 1999, which was conducted in the Cessna T303. AIRCRAFT INFORMATION On April 30, 1994, the left engine was removed from the airplane and overhauled. During the overhaul, all steel parts were magnafluxed, and all aluminum parts were zygloed. The engine was then re-installed on the airplane. The engine's total time at overhaul was 3,596 hours and it had accumulated about 1,874 hours since. The last maintenance performed on the engine was on October 20, 1999. It included an oil change and oil filter replacement. METEOROLOGICAL INFORMATION The weather reported by BGM at 0608 was; winds calm, 1/4 statute mile of visibility, fog, vertical visibility of 100 feet, temperature and dew point of 45 degrees Fahrenheit. WRECKAGE AND IMPACT INFORMATION The wreckage was examined on November 1, 1999, at the accident site. The airplane came to rest on Runway 34; about 1,900 feet from the approach end, on a heading of about 290 degrees, and at an elevation of 1,636 feet mean sea level. All major components of the airplane were accounted for at the accident site. The nose landing gear was collapsed, and exhibited scaring along the left side of the wheel forks. The forward nose cone section was crushed upward and to the right. It displayed scraping along the underside. The main landing gear were extended and locked. The right outboard wing section, which was exposed to a post crash fire, exhibited rearward buckling, and damage along the wing tip. All control cables and fuel lines remained connected between the wing firewall and the right engine. Powerplant control cable continuity was confirmed from the cockpit to the engine. The right engine throttle lever, propeller control, and mixture control, were all found in the full forward position. Fuel was observed draining from the fuel lines as the engine was removed from the fuselage. The right wing fuel tank was not damaged and contained an undetermined amount of fuel. The outboard section of the left wing exhibited damage from the impact and post crash fire. All control cables and fuel lines remained connected between the wing firewall and the left engine. Powerplant control cable continuity was confirmed from the cockpit to the engine. The left engine throttle lever, and propeller control were found in the full aft position. The mixture control was found in the mid-range position. A small amount of fuel was observed draining from the fuel lines as the engine was removed from the fuselage. The left wing fuel tank was compromised and did not contain any fuel. Flight control continuity was confirmed from the cockpit area to the ailerons, rudder, and elevator. The flaps were found in the full extend position, which corresponded with the selector position located in the cockpit. The left engine was inspected after being removed from the wreckage. It exhibited damage due to the post-crash fire. The engine was rotated by hand, using the propeller. Some resistance was noted during the rotation. The number 6 cylinder was damaged during the impact sequence and displayed exposed valves. Thumb compression was only confirmed to the number 3 and 5 cylinders. No compression could be determined for the remaining four cylinders. The top and bottom spark plugs were removed; their electrodes were intact and light gray in color. The left and right magnetos were removed from the engine and rotated by hand, producing spark on all towers. While the engine was rotated, the accessory drive section gears and the number 1 and 2 cylinder valves did not show any signs of movement. The propeller remained attached to the engine. Two of the three propeller blades were in the feather position. The remaining blade was in a high pitch position and bent 90 degrees about 9 inches from the hub. The counterweight for the bent propeller blade was found detached from the hub and was located along the debris path. The fuel manifold valve on the left engine was inspected. The diaphragm was dry, but exhibited a smell of aviation fuel. The fuel screen was free of debris. The fuel selector control for the left tank was found in the crossfeed position, and the right tank selector was in-between the on and off positions. TESTS AND RESEARCH The airplane's left engine was examined at Hagerstown, Maryland, on December 8, 1999, under the supervision of a Safety Board Investigator. Removal of the engine oil sump revealed large pieces of metal and metal shavings in the sump and trapped in the oil sump suction screen. Disassembly of the engine revealed that the crankshaft was fractured between connecting rod journal number 2 and main journal number 2. The crankshaft was forwarded to the Safety Board's materials lab on December 9, 1999. Fracture surfaces on the crankshaft were examined by optical microscopy. The fracture surface on the aft section of the crankshaft was destroyed by post-fracture damage. The fracture surface on the forward section of the crankshaft displayed several areas of smooth features, curving boundaries, and ratchet marks, all typical of fatigue. ADDITIONAL INFORMATION Review of the Cessna T303 pilot's operating handbook revealed that the single engine service ceiling, at a weight of 4,800 pounds, with the landing gear and flap in the retracted position, was 11,700 feet. The average single engine rate of climb, at a pressure altitude of 6,000 feet, a temperature of -5 degrees centigrade, and a weight of 4,800 pounds, was 295 feet per minute. The average single engine rate of climb, at a pressure altitude of 1,625 feet, a temperature of 7.5 degrees centigrade, and a weight of 4,800 pounds, was 314 feet per minute. Review of the ILS approach plate for Runway 34 revealed that the decision height was 200 feet above the ground. The airplane wreckage was released on November 1, 1999, to a representative of the owner's insurance company.
The pilot's improper in-flight decision to descend below the decision height without the runway environment in sight, and his failure to execute a missed approach. A factor in the accident was the failed crankshaft.
Source: NTSB Aviation Accident Database
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