SHELBYVILLE, IN, USA
N84DG
Ellis Q2
A witness to the accident reported that during an attempted go-around the airplane's engine was missing and running rough. The witness stated that the airplane entered a descending left turn, impacting the terrain in a 30-45 degree left bank. Post accident inspection of the airplane revealed that the main and header fuel tanks had ruptured, but no fuel spill or fuel odor was noted at the accident site. Witnesses/first responders to the accident site reported that there were no fuel odors around the accident site. Inspection of the engine failed to reveal any anomalies that could be associated with any preexisting condition. A fuel receipt was obtained for the accident airplane's last fueling. The date of the fuel receipt was listed as November 28, 1999, and 6.2 gallons of fuel were purchased for the accident airplane.
On February 25, 2000, at 1335 eastern standard time (est), an Ellis Q2, N84DG, owned and piloted by an airline transport pilot, was destroyed during an in-flight collision with terrain following a loss of control during a go-around from runway 19 (5,000 feet by 100 feet, dry/asphalt) at the Shelbyville Municipal Airport, Shelbyville, Indiana. Visual meteorological conditions prevailed at the time of the accident. The personal flight was operating under the provisions of 14 CFR Part 91 and was not on a flight plan. The pilot, the sole occupant, was fatally injured. The local flight originated from the Shelbyville Municipal Airport approximately 20 minutes prior to the accident. According to a pilot-rated witness, the airplane was on final approach for runway 19 when the airplane began a go-around. The witness described the engine operation, during the go-around, as "missing and running rough". The witness reported that the airplane entered a descending left turn, impacting the terrain in a 30-45 degree left bank. Post accident inspection of the airplane revealed that the main and header fuel tanks had ruptured, but no fuel spill or fuel odor was noted at the accident site. Witnesses/first responders to the accident site reported that there were no fuel odors around the accident site. Inspection of the engine failed to reveal any anomalies that could be associated with any preexisting condition. A fuel receipt was obtained for the accident airplane's last fueling. The date of the fuel receipt was listed as November 28, 1999, and 6.2 gallons of fuel were purchased for the accident airplane. An autopsy was performed on the pilot on February 26, 2000, at the Indiana University School of Medicine, Indianapolis, Indiana. The Federal Aviation Aeromedical Institute, Oklahoma City, Oklahoma, prepared a forensic toxicology report. The test results indicated that there was 0.011 (ug/ml, ug/g) Tetrahydrocannabinol (Marijuana) detected in lung tissue, and that Tetrahydrocannabinol Carboxylic Acid (Marijuana metabolite) was detected in blood and lung tissue.
aircraft control not being maintained by the pilot during the attempted go-around. Factors to the accident were the inadequate preflight by the pilot, which resulted in fuel exhaustion. An additional factor to the accident was the inadvertent stall/mush.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports