Aviation Accident Summaries

Aviation Accident Summary DEN00LA091

LARKSPUR, CO, USA

Aircraft #1

N758SZ

Cessna 172XP

Analysis

During a dual instructional flight, the flight instructor gave the student a practice engine out approach by reducing power to 'just above idle.' At the completion of the maneuver, the student added power and the engine failed to respond. The instructor took control and conducted a forced landing to the field the student was using as a target for his maneuver. The terrain was soft and the aircraft nosed over during landing roll. Examination of the aircraft/engine, provided evidence the boost pump was improperly wired giving high boost when either high or low was selected. The switch was found on the low selection as prescribed for the maneuver being conducted. When and who made the wiring change was not determined.

Factual Information

On May 19, 2000, at 0955 mountain daylight time, a Cessna 172XP, N758SZ, sustained substantial damage during a forced landing near Kelly Air Park (U38), Larkspur, Colorado, when it nosed over on landing roll. The certified flight instructor and student pilot were not injured and no flight plan was filed for this instructional flight operating under Title 14 CFR Part 91. The flight departed Centennial Airport, Englewood, Colorado, at 0900. Visual meteorological conditions prevailed. According to the flight instructor, he reduced power to "just above" idle approximately 2,000 feet above ground level (agl) and was having his student practice an engine out approach. The student set up for approach to an open field and the flight instructor said he checked the engine once during the glide, which was described as being in excess of 2 miles. When the student added power at the termination of the approach, the engine failed to respond. The instructor said he took control of the aircraft and decided to land in the field the student had picked during practice. The field was soft and muddy and during landing roll, the nose landing gear dug in and the aircraft nosed over causing substantial damage to the wings, fuselage, and empennage. Examination of the aircraft/engine provided no evidence of an airframe or engine abnormality. It did provide evidence that the fuel boost pump had been improperly wired so that it operated in high if either the "low" or "high" on position was selected. When the wiring was done was not established, and the mixture setting being used by the pilot was also not established. The boost pump switch was found in the "low" position as prescribed for the maneuver being conducted. The closest weather reporting station, approximately 10 miles from the accident site, recorded a temperature of 82 degrees Fahrenheit and a dew point of 55 degrees Fahrenheit during the time period when the accident took place.

Probable Cause and Findings

A forced landing on soft unsuitable terrain. Factors were improper wiring of the electric fuel boost pump, which produce high pressure when either on position was selected causing the engine to flood during the practice engine out approach.

 

Source: NTSB Aviation Accident Database

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