OAKDALE, MN, USA
N5120B
BELL 47
WHILE FERRYING THE HELICOPTER TO CONDUCT AN AERIAL APPLICATION OPERATION, THE PLT SAID THAT THE ENGINE BEGAN TO OVERSPEED. THE PLT ENTERED AN AUTOROTATION TO REDUCE ENGINE RPM, BUT HAD TO CLEAR POWER LINES. USING THE ROTOR RPM TO CLEAR THE POWER LINES, THE ROTOR RPM DECAYED AND THE ACFT DROPPED IN FROM ABOUT 50 TO 75 FEET AGL. POST ACCIDENT INVESTIGATION REVEALED A MALFUNCTIONING MAIN TRANSMISSION CENTRIFUGAL CLUTCH. THE POWERPLANT TEST FAILED TO REVEAL ANY MALFUNCTION. AN ANNUAL INSPECTION HAD BEEN PERFORMED 6 DAYS AND 4 HOURS OF FLIGHT TIME PRIOR TO THE ACCIDENT.
A SLIPPING ROTOR DRIVE CLUTCH ASSEMBLY DUE TO IMPROPER MAINTENANCE BY COMPANY PERSONNEL. CONTRIBUTING FACTORS WERE STATIC WIRES IN THE PATH.
Source: NTSB Aviation Accident Database
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