Aviation Accident Summaries

Aviation Accident Summary FTW90LA136

WHARTON, TX, USA

Aircraft #1

N351WB

CESSNA T210M

Analysis

THE PILOT STATED THAT HE TURNED THE AUX FUEL PUMP ON WHILE ON DOWNWIND, SWITCHED TO THE FULLEST TANK, AND THEN TURNED THE AUX FUEL PUMP OFF. HE ALSO STATED THAT AT 400 FEET ON FINAL HE PUT THE FLAPS DOWN, AND TRIED TO INCREASE POWER. HE RECEIVED NO ENGINE RESPONSE. AFTER EMERGENCY PROCEDURES FAILED HE MADE A FORCED LANDING, AND THE AIRPLANE NOSED OVER IN A MUDDY FIELD. INVESTIGATION REVEALED AN OUT-OF-RIG CONDITION ON THE THROTTLE RELATED SYSTEM THAT AUTOMATICALLY CONTROLLED THE TWO POSITION/PRESSURE AUX FUEL PUMP. ENGINE RUN BEFORE RE-RIGGING REVEALED AN OVER RICH MIXTURE AND ROUGH ENGINE AT IDLE; BEYOND 1/3 THROTTLE THE ENGINE WOULD NOT RUN. ENGINE RUN AFTER RE- RIGGING REVEALED NORMAL OPERATION. THE PILOT'S CHECKLIST STATES 'AUXILIARY FUEL PUMP - OFF,' THREE LINES AFTER STATING 'FUEL SELECTOR VALVE - FULLER TANK.'

Probable Cause and Findings

THE LOSS OF POWER DUE TO AN OUT-OF-RIG CONDITION IN THE AUTOMATIC AUXILIARY BOOST PUMP MECHANISM.

 

Source: NTSB Aviation Accident Database

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