Aviation Accident Summaries

Aviation Accident Summary ANC90LA135

TOK, AK, USA

Aircraft #1

N58000

AEROSPATIALE SA-315B

Analysis

THE HELICOPTER WAS BEING USED IN AN EXTERNAL LOAD OPN TO CARRY CARGO WITH A 100 FT CABLE. WHILE HOVERING OUT OF GROUND EFFECT, THE ENG LOST PWR. A SUBSEQUENT HOVERING AUTOROTATION RESULTED IN A HARD LANDING. AN EXAM REVEALED THE LOSS OF POWER WAS DUE TO FUEL CONTAMINATION ALTHOUGH AN AIRFRAME FUEL FILTER WAS INSTALLED IN THE MAIN FUEL SUPPLY LINE. AN EXAM REVEALED THE FILTER ELEMENT HAD BEEN INSTALLED BACKWARD IN THE FILTER CANISTER. THIS ALLOWED CONTAMINATED FUEL TO BYPASS THE FILTER ELEMENT & ENTER THE ENG FUEL CTL UNIT. THE REVERSE INSTLN ALSO RESULTED IN AN INOP 'FUEL FILTER CLOGGED' WARNING LGT & PREVENTED THE PRESSURE DIFFERENTIAL BUTTON ON THE FILTER HOUSING FM EXTDG. THE FILTER HAD BEEN INSPECTED & REINSTLD DRG A 100 HR INSPN, 17 FLT HRS BFR THE ACDNT. THIS WORK WAS DONE BY A PLT UNDER SUPERVISION OF A MECHANIC. THE MECHANIC HAD NO PREV EXPERIENCE WITH THIS MAKE & MODEL OF HELICOPTER. 'TOP' & 'BOTTOM' WERE STENCILED ON THE FILTER ELEMENT IN FRENCH. CONTAMINATED FUEL WAS ALSO FND IN THE FUEL TRUCK.

Probable Cause and Findings

IMPROPER INSTALLATION OF THE FUEL FILTER ELEMENT IN THE AIRCRAFT BY COMPANY/MAINTENANCE PERSONNEL, AND SUBSEQUENT CONTAMINATION OF THE FUEL SYSTEM BY UNFILTERED FUEL. FACTORS RELATED TO THE ACCIDENT WERE: INADEQUATE DESIGN OF THE FUEL FILTER ASSEMBLY, WHICH ALLOWED THE IMPROPER INSTALLATION OF THE FILTER ELEMENT, THE MECHANICS LACK OF FAMILIARITY WITH THE AIRCRAFT, AND FAILURE OF GROUND PERSONNEL TO INSURE THAT FUEL FROM THE FUEL TANKER WAS FREE OF CONTAMINATION.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports