Aviation Accident Summaries

Aviation Accident Summary FTW90FA170

SHREVEPORT, LA, USA

Aircraft #1

N6132S

Air & Space 18A

Analysis

THE PIC STATED THAT AT LIFTOFF A SEVERE LATERAL VIBRATION OCCURRED CAUSING LOSS OF CONTROL OF THE GYROPLANE. WITNESSES REPORTED AN ERRATIC PORPOISING PITCHING MOTION. THE AIRCRAFT CAME TO REST APPROXIMATELY 1,500 FEET AFTER CONTROL WAS LOST, WHICH WAS AT THE POINT OF ATTEMPTED LIFTOFF. AS A RESULT OF FLAPPING, TWO OF THE THREE ROTOR BLADES CONTACTED THE PROPELLER AND RUDDER. ALTHOUGH NOT RECOMMENDED BY THE MANUFACTURER, THE FRONT SEAT WAS OCCUPIED BY A PILOT RATED PASSENGER WITH NO GYROPLANE EXPERIENCE. DURING SUBSEQUENT FLIGHT TESTING, TAKEOFF WAS PERFORMED UNDER SIMILAR CONDITIONS. IMPROPER TECHNIQUES DURING ATTEMPTED LIFTOFF RESULTED IN ERRATIC OSCILLATION AND ROTOR RPM DECAY. NO MECHANICAL MALFUNCTION WAS DISCOVERED.

Probable Cause and Findings

FAILURE OF THE PILOT IN COMMAND TO FOLLOW PUBLISHED TAKEOFF PROCEDURES.

 

Source: NTSB Aviation Accident Database

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