SUFFOLK, VA, USA
N7702B
AERONCA CHAMPION 7BCM
THE ACFT WAS CLIMBING OUT AFTER THE SECOND TOUCH-AND-GO LANDING, WHEN WITNESSES REPORTED HEARING POPPING NOISES FROM THE ENGINE. THE ACFT NOSED DOWN, DESCENDED, AND CRASHED IN A WOODED AREA ABOUT 1,000 FT PAST THE END OF THE RWY. INVESTIGATION REVEALED A COMPRESSION TEST READING OF 17/80 FOR THE #2 CYLINDER; THE EXHAUST VALVE GUIDE AND SEAT WERE MISALIGNED. IN ADDITION, ALL THE ENGINE INTAKE CONNECTOR HOSES WERE DRY-ROTTED, THE SPARK PLUGS APPPEARED TO BE GAPPED TOO TIGHTLY, AND ONE LEAD WAS NOT PROPERLY INSTALLED. THE LAST ANNUAL INSPECTION WAS DONE ABOUT A WEEK BEFORE THE ACCIDENT, AND THE ACFT HAD OPERATED ABOUT 15 HRS SINCE THEN.
A LOSS OF ENGINE POWER DUE TO LOW CYLINDER COMPRESSION. THE LOW COMPRESSION WAS A RESULT OF EXHAUST VALVE LEAKAGE AND INADEQUATE MAINTENANCE AND INSPECTION. IN ADDITION, THE PILOT FAILED TO MAINTAIN ADEQUATE AIRSPEED WHICH RESULTED IN THE AIRPLANE STALLING.
Source: NTSB Aviation Accident Database
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