LOUISVILLE, KY, USA
N9280F
HUGHES 269C
THE PILOT WAS PATROLLING A PIPELINE WHEN THE ENGINE LOST POWER. HE DID AN AUTOROTATION LANDING IN AN OPEN FIELD. THE INVESTIGATION REVEALED THE NUMBER ONE CYLINDER CONNECTING ROD CAP HAD FRACTURED. METALLURGICAL EXAMINATION OF THE FRACTURE SURFACE REVEALED A FATIGUE CRACK HAD ORIGINATED FROM A GALLING MARK ON THE BEARING SURFACE OF THE ROD. THE ENGINE WAS OPERATED 39 HOURS SINCE IT WAS LAST OVERHAULED.
FATIGUE FAILURE OF THE NUMBER 1 CYLINDER CONNECTING ROD.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports