LAKELAND, FL, USA
N81562
BEECH F33A
BEFORE DEPARTURE, THE PLT PREFLIGHTED THE ACFT & PERFORMED AN ENG RUN-UP WITH NO DISCREPANCIES NOTED. AFTER DEPARTURE WHILE CLIMBING THROUGH 5,500 FT, THE ENG QUIT. THE PLT RESTARTED THE ENG BUT OBSERVED THE OIL PRESSURE WAS ZERO. THE ENG QUIT AGAIN & HE WAS UNABLE TO RESTART IT. DURING THE FORCED LANDING IN A FIELD, THE ACFT COLLIDED WITH A TREE. EXAM OF THE ACFT REVEALED OIL COATING THE BOTTOM OF THE FUSELAGE. THE ENG COMPARTMENT WAS NOT CONTAMINATED. THE ENG WAS REMOVED & EXAM OF IT REVEALED THAT THE NO'S 1,2,5, & 6 PISTONS SCORED THE CYLINDER WALLS. NO'S 3 & 4 PISTONS WERE NORMAL. DUE TO THE DAMAGE, NO DIMENSIONAL ANALYSIS OF THE FAILED PISTONS & CYLINDERS COULD BE MADE. THE ENG DRIVEN OIL PUMP WAS EXAM & FOUND TO BE FREE OF FAILURE OR MALFUNCTION. NO DETERMINATION COULD BE MADE AS TO THE REASONS FOR THE LOSS OF ENG OIL RESULTING IN THE TOTAL LOSS OF ENG POWER DUE TO SEIZURE OF THE NO'S 1,2,5, & 6 PISTONS IN THE CYLINDERS. THE ACFT & ENG HAD ACCUMULATED 16.1 HRS SINCE MANUFACTURE.
TOTAL LOSS OF ENGINE POWER DUE TO OIL EXHAUSTION FOR UNDETERMINED REASONS. THIS CAUSED THE PISTONS TO SEIZE IN THE CYLINDERS.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports