MINEOLA QUITMAN, TX, USA
N3709X
AERO COMMANDER 100-180
DURING A PRACTICE TOUCH AND GO LANDING, THE ENGINE BACK FIRED AND THEN SURGED. AT ABOUT 150' AGL THE ENGINE RPM DROPPED ABOUT 80% AND THE PILOT ATTEMPTED TO MAKE AN EMERGENCY LANDING IN AN OPEN FIELD. THE AIRCRAFT FLEW OVER A TRASH DUMP AND BETWEEN TWO TREES. WHILE ATTEMPTING TO CLEAR A FENCE THE STALL WARNING HORN WENT OFF. THE AIRCRAFT CONTACTED THE GROUND LEFT MAIN AND WING FIRST CAUSING SUBSTANTIAL DAMAGE. EXAMINATION OF THE ENGINE FOUND THAT THE ENGINE EXHAUST MUFFLER HAD FAILED INTERNALLY BLOCKING THE EXHAUST OUTLET.
Source: NTSB Aviation Accident Database
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