WHEELER, IN, USA
N8568A
BEECH A35
THE ACFT WAS BEING OPERATED IAW A FERRY PERMIT TO OBTAIN AN ANNUAL INSPN. THE PREV ANNUAL INSPN WAS ON 3/13/85. DRG FLT ABT 1.3 HRS AFTER TAKEOFF, THE ENG LOST PWR. THE PLT NOTED THE FUEL PRES WAS ZERO. HE SAID HE TURNED ON THE AUX FUEL PUMP & INSURED THE FUEL SEL WAS PSND TO THE LEFT TANK WHICH HAD A FULL INDCN. HE ALSO OPERATED THE WOBBLE PUMP, BUT GOT NO FUEL PRES, EXCEPT FUEL PRES & ENG POWER WERE OBTAINED FOR SVRL SHORT PERIODS OF TIME, BUT PWR COULD NOT BE SUSTAINED. SUBSEQUENTLY, THE ACFT WAS EXTENSIVELY DAMAGED DRG A FORCED LNDG ON A FROZEN, SNOW COVERED, CORN FIELD. THE ACFT WAS MOVED & DISASSEMBLED BEFORE THE INVESTIGATOR COULD CHECK THE FUEL SYS.
Source: NTSB Aviation Accident Database
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