CHEYENNE, WY, USA
N910DS
CESSNA 210L
THE CFI WAS GIVING A CHECKOUT TO THE PRIVATE PILOT DOCTOR. THE CFI FLIGHT RECORDS SHOWED ONLY ONE HOUR IN THIS MAKE/MODEL. THE FUEL SELECTOR WAS IN THE RIGHT TANK POSITION THROUGHOUT THE FLIGHT. THE PILOT REPORTED THAT THE ENGINE QUIT ON ONE MILE SHORT FINAL FOR RUNWAY 26 AT CHEYENNE, MUNICIPAL. A POST ACCIDENT INSPECTION AND ENGINE RUN FAILED TO REVEAL EVIDENCE OF A MECHANICAL ENGINE PROBLEM. NEITHER PILOT COULD REMEMBER SWITCHING TANKS DURING THE EMERGENCY, OR DURING THE RESTART ATTEMPT. POST INVEST REVEALED THAT THE ACFT LANDED ON A HIWAY. DURING LNDG THE ACFT STRUCK A CURB, A CHAIN LINK FENCE AND A LIGHT POLE. THE ACFT SKIDDED TO A STOP AFTER THE LNDG GEAR COLLAPSED. THE ACFT RT FUEL TANK HAD BEEN RUPTURED BUT ONLY A SMALL AMOUNT OF FUEL SPILLED. THE CREW WAS PRACTICING ILS APPROACHING WHEN THE ENG QUIT.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports