WAYSIDE, MS, USA
N7961
GRUMMAN G-164A
WHILE ON AN AERIAL APPLICATION FLT ON SHORT FINAL, THE PLT PULLED THE THROTTLE LEVER TO REDUCE AIRSPEED BUT IT BROKE AT THE POWER CONTROL QUADRANT. THE APCH WAS CONTINUED & AFTER ACFT TRAVELED APRX 1/2 THE LENGTH OF THE RWY, HE TURNED THE MAGNETO SWITCH OFF. THE ACFT TOUCHED DOWN NEAR OBSTRUCTIONS & OCCUPIED VEHICLES AT THE DEPARTURE END OF THE RWY, THE PLT INTENTIONALLY PUSHED THE CONTROL STICK FWD WHICH CAUSED THE ACFT TO NOSE OVER & COME TO REST INVERTED.
Source: NTSB Aviation Accident Database
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