LOWELL, AR, USA
N3738X
AERO COMMANDER 100-180
ABOUT ONE HOUR AFTER TAKEOFF, THE PLT NOTED THAT THE ENG BEGAN TO RUN ROUGH. HE REDUCED THE POWER TO 2000 RPM & ENRICHED THE MIXTURE. HE CONTINUED FLYING FOR ABOUT ANOTHER HOUR, THEN THE ENG LOST POWER. THE PLT ATTEMPTED AN EMERGENCY LANDING ON A FRONTAGE ROAD, BUT WAS UNABLE TO REACH IT. THE ACFT WAS DAMAGED WHEN IT TOUCHED DOWN ON ROUGH TERRAIN JUST SHORT OF THE ROAD. AN EXAM REVEALED THE EXHAUST & INTAKE VALVES AT THE #4 CYLINDER HAD STUCK.
Source: NTSB Aviation Accident Database
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