MINNEAPOLIS, MN, USA
N729RW
BOEING 727-200
AFTER PUSHBACK FROM THE JETWAY, THE AIRPLANE HIT A GROUND HANDLING VEHICLE (TUG) AS THE FLT CREW STARTED TO TAXI FOR TAKEOFF. AN INVESTIGATION REVEALED THAT AFTER PUSHBACK, THE GROUND CREW INFORMED THE FLT CREW (VIA INTERCOM) THAT THE BYPASS PIN WAS REMOVED & THE STEERING WAS CONNECTED. THE GROUND CREWMAN ENDED THE CONVERSTATION BY STATING 'YOU GENTLEMEN HAVE A NICE TRIP, SEE YOU ANOTHER DAY.' THE INTERCOM WAS DISCONNECTED & THE CAPTAIN STARTED TO TAXI, BEFORE RECEIVING A VISUAL SIGNAL FROM THE GROUND CREW & BEFORE THE TUG WAS REMOVED FROM THE AIRPLANE'S PATH. SUBSEQUENTLY, THE AIRPLANE HIT THE TOP OF THE TUG & DAMAGED THE LOWER RIGHT PART OF THE FORWARD FUSELAGE (BELOW THE COCKPIT WINDOWS).
FAILURE OF THE CAPTAIN TO FOLLOW COMPANY PUSHBACK PROCEDURES AND NOT GETTING A RELEASE BEFORE STARTING TO TAXI.
Source: NTSB Aviation Accident Database
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