Aviation Accident Summaries

Aviation Accident Summary LAX88FA321

BIG BEAR, CA, USA

Aircraft #1

N55478

PIPER PA-28-140

Analysis

THE NIGHT BEFORE THE ACCIDENT THE PLT & 2 PAX WENT GAMBLING. THEY RETIRED FOR THE EVENING (MORNING) BETWEEN 0315 & 0400. THEY AWOKE AT ABOUT 0830. AT 1007 THEY FLEW FM BULLHEAD, AZ TO BIG BEAR, CA. WHEN THE PLT ATTEMPTED TO DEPART FM THE BIG BEAR ARPT HE LEFT THE MIXTURE CONTROL IN THE FULL RICH POSITION. AS THE ACFT TRANSITIONED OUT OF GROUND EFFECT IT STALLED. THE PLT HELD THE YOKE AFT AS THE ACFT ENTERED AN UNCONTROLLED DESCENT & CRASHED 1880 FT BEYOND THE RUNWAY'S END. THE FRONT RIGHT SEATED PAX VIDEO TAPED THE ACCIDENT FLIGHT. THE 93-HR TOTAL TIME PLT HAD 33-HRS IN MAKE & MODEL ACFT. NO EVIDENCE WAS FOUND OF HIM HAVING RECEIVED DUAL INSTRUCTION IN HIGH DENSITY ALTITUDE TAKEOFFS. THE DA WAS IN EXCESS OF 8500 FT. THE ACFT'S CERTIFICATED MAX GROSS WEIGHT WAS EXCEEDED. A BOX CONTAINING MARIJUANA WAS FOUND IN THE ACFT WRECKAGE. TOX RESULTS CONFIRMED MARIJUANA IN THE PLT'S BLOOD & IN THE CAMERMAN/PAX'S URINE.

Probable Cause and Findings

THE PILOT FAILED TO MAINTAIN AIRSPEED DURING TAKEOFF. CONTRIBUTING FACTORS RELATED TO THE HIGH DENSITY ALTITUDE CONDITION, THE AIRCRAFT'S EXCESSIVE WEIGHT AND THE PILOT'S FAILURE TO LEAN THE MIXTURE. ALSO CONTRIBUTING TO THE ACCIDENT WAS THE PILOT'S IMPROPER REMEDIAL ACTION TO AFFECT RECOVERY FROM THE DEVELOPING STALL, HIS POOR JUDGEMENT, HIS LACK OF EXPERIENCE IN THE AIRPLANE, AND HIS IMPAIRED PHYSIOLOGICAL CONDITION AS IT RELATED TO HIS LACK OF SLEEP AND DRUG USE.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports