AUSTELL, GA, USA
N83045
AERONCA 7AC
PIC WAS OBTAINING BFR; STALLS & FLT AT MIN CONTROL AIRSPEED WERE COMPLETED. PIC BEGAN DESCENT FROM 2500 MSL TO HIS PVT STRIP FOR SIMULATED ENGINE OUT LANDING. IN A SUBSEQUENT INTERVIEW PIC SAID CARB HEAT WAS APPLIED & REMOVED AFTER 30 SEC. IN HIS RPT HE SAID CARB HEAT WAS REMOVED WHEN INSTRUCTOR SAID MANEUVER WAS COMPLETED. ON BASE LEG INSTRUCTOR INDICATED MANEUVER HAD BEEN COMPLETED. PIC APPLIED POWER TO 1700 RPM, THEN 1800 RPM, & FLEW OVR RWY 33 AT 2,300 FEET AGL. WHEN POWER WAS APPLIED TO CLIMB, ENGINE SPUTTERED & LOST POWER. PIC MADE A 270 DEGREE TURN TO LEFT TO ATTEMPT TO LAND IN A LAND FILL. AFTER ABOUT 200 DEGREES OF TURN THE NOSE OF THE ACFT YAWED RIGHT. THE ACFT STALLED AND IMPACTED IN A CUDZU PATCH ADJACENT TO RWY. BOTH PILOTS STATED THAT THE BFR HAD BEEN COMPLETED AND THAT THE PILOT/OWNER WAS THE PIC.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports