WALLINGFORD, CT, USA
N555GC
BELL 206L-1
THE ACFT LOST POWER AND CRASHED IN A TRACTOR TRAILER PARKING LOT, DESTROYING THE HELICOPTER AND CAUSING SERIOUS INJURIES TO THE PILOT AND ONE PASSENGER. THE INVESTIGATION REVEALED AN IMPROPER FUEL FLOW SWITCH, WHICH HAD NO CHECK VALVE PROTECTION INSTALLED ON SYSTEM NO 1. THE FAA CERTIFICATION BRANCH (ASW-170) STATED THAT IF THE WRONG FUEL FLOW SWITCH IS USED AND THE BOOST PUMP CIRCUIT BREAKERS ARE PULLED, A FLAMEOUT IS LIKELY. THE PILOT SAID HE PULLED THE MASTER CAUTION BREAKER AND MAY HAVE PULLED THE BOOST PUMP BREAKERS 'PREPARING FOR LANDING'. THE FUEL BOOST PUMP CIRCUIT BREAKERS WERE PULLED AND THERE WERE APPROXIMATELY 27 GAL OF FUEL REMAINING, WHEN THE ENGINE QUIT.
Source: NTSB Aviation Accident Database
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