LIANO, CA, USA
N85HL
MARTIN SORRELL HIPERLIGHT
AN ENGINE FAILURE OCCURRED SHORTLY AFTER TAKEOFF. DISASSEMBLY OF THE ENGINE REVEALED THE PISTON HAD SEIZED WITH FOUR POINTS OF CONTACT ALONG THE CYLINDER WALL. THE ENGINE HAD BEEN RECENTLY OVERHAULED AND HAD 1.1 TOTAL HOURS AT THE TIME OF THE ACCIDENT. THE TWO CYCLE ENGINE (MANUFACTURERED BY ROTAX) HELD NO FAA APPROVAL BY EITHER TYPE CERTIFICATE OR PRODUCTION CERTIFICATE.
ENGINE FAILURE DUE TO A SEIZED PISTON.
Source: NTSB Aviation Accident Database
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