MIAMI, FL, USA
N704XE
CESSNA 152
THE PLT STATED THAT HE WAS CRUISING ALONG THE COASTLINE AT ABOUT 600 FT AGL, WHEN THE ENG BEGAN TO LOSE POWER & RUN ROUGH. A FORCED LDG WAS PERFORMED WHEN THE PLT REALIZED THERE WAS INSUFFICIENT POWER AVAIL TO SUSTAIN FLT. SUBSEQUENTLY, THE ACFT TOUCHED DOWN ON ROUGH TERRAIN & NOSED OVER. AN EXAM OF THE ENG REVEALED THAT THE ROCKER SHAFT BOSS ON THE #3 CYLINDER HAD FAILED.
FAILURE OF A ROCKER SHAFT BOSS ON THE NUMBER THREE CYLINDER. A RELATED FACTOR WAS THE ROUGH TERRAIN IN THE EMERGENCY LANDING AREA.
Source: NTSB Aviation Accident Database
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