ROSEAU, MN, USA
N23702
AIR TRACTOR AT-301
THE PLT SAID THAT SHORTLY AFTER TAKEOFF AND REACHING AN ALTITUDE OF ABOUT 500 FT AGL, THE ENGINE QUIT. HE SAID HE WAS ABLE TO GET SEVERAL SHORT BURSTS OF POWER BY OPERATING THE HAND FUEL PUMP, BUT WAS UNABLE TO SUSTAIN ENGINE POWER. AN EMERGENCY LDG WAS ATTEMPTED IN A SWAMP AREA WHICH RESULTED IN THE ACFT NOSING OVER. THE PLT FELT THERE WAS A POSSIBILITY OF ICE IN THE FUEL LINES DUE TO THE EXISTING SUB-FREEZING TEMPERATURE. THE PLANE WAS BEING FLOWN TO ANOTHER APT FOR AN ANNUAL INSPECTION.
FUEL STARVATION DUE TO FUEL ICE.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports