Aviation Accident Summaries

Aviation Accident Summary MKC89LA118

STRONG, AR, USA

Aircraft #1

N18307

BEECH V35

Analysis

ABOUT 25 MILES FROM DESTINATION APT, THE PLT SAID THE ENGINE QUIT. HE SWITCHED FROM EMPTY LEFT TANK TO THE RIGHT TANK, WHICH STILL INDICATED 1/2 TO 3/4 FULL. HE WAS UNABLE TO RESTART THE ENGINE, AND DUE TO HIS ALTITUDE OF 1500 AGL, ELECTED TO MAKE AN EMERGENCY LDG. DURING THE LANDING ON A RURAL GRAVEL ROAD, THE ACFT SUSTAINED SUBSTANTIAL DAMAGE. THE PLT SAID THAT THE LEFT FUEL CELL BLADDER HAD BEEN REPLACED 3 DAYS PRIOR TO THE ACCIDENT, DUE TO PREVIOUS LEAKS, BUT DOCUMENTATION OF THE REPLACEMENT WAS NOT FOUND BY THE INVESTIGATIVE AUTHORITIES.

Probable Cause and Findings

ENGINE FAILURE DUE TO FUEL STARVATION.

 

Source: NTSB Aviation Accident Database

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