ANCHORAGE, AK, USA
N8773Q
CESSNA U-206G
THE ACCIDENT REPORT SUBMITTED BY THE FLYING CLUB CHIEF INDICATED THAT THE PILOT DID NOT RELEASE THE TAIL TIEDOWN DURING HIS PREFLIGHT INSPECTION. IT WAS ATTACHED TO A 4X4 POST IN A CONCRETE WEIGHT. DURING THE ATTEMPTED TAKEOFF THE AIRPLANE WOULD NOT GET ON STEP. THE TAKEOFF WAS ABORTED. A SECOND TAKEOFF WAS ATTEMPTED FROM THE MIDDLE OF THE LAKE. DURING THE TAKEOFF THE NOSE BEGAN TO PITCH UP APPROACHING A STALL. THE PILOT PUSHED THE YOKE FORWARD & THE AIRPLANE SETTLED BACK ONTO THE WATER JUST PRIOR TO IMPACT WITH THE LAKE'S DEPARTURE END SHORELINE.
THE FAILURE OF THE PILOT TO CONDUCT A PROPER PRE-FLIGHT INSPECTION AND REMOVE THE TAIL MOORING FROM THE FLOAT PLANE. CONTRIBUTING TO THE ACCIDENT WAS THE PILOT'S OVER CONFIDENCE IN HIS PERSONAL ABILITY.
Source: NTSB Aviation Accident Database
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