HIGHGATE, VT, USA
N3496X
MOONEY M20C
ACCORDING TO THE SURVIVING PAX, A SNOWSHOWER WAS ENCTRD, SO THE PLT REVERSED COURSE & DIVERTED TO ANOTHER ARPT. DRG A NGT APCH TO LND, THE PAX NOTED A WHITE LIGHT ON THE LEFT SIDE OF THE RWY. (A VASI LIGHT SYS WAS INSTALLED FOR THAT RWY.) THE PLT ABORTED THE LNDG, BUT DRG A GO-AROUND, THE ACFT STRUCK TREETOPS APRX 1500' BEYOND THE DEP END OF THE RWY & CRASHED. NO PREIMPACT PART FAILURE OR MALFUCTION WAS EVIDENT. THE LNDG GEAR & GEAR HANDLE WERE FND IN THE DOWN PSN, THE FLAPS WERE IN A RETRACTED PSN & THE ENG CTLS WERE FND AT FULL POWER SETTINGS. ONLY 3.4 HRS OF THE PLT'S FLT TIME WAS RPRTD IN HI PERFORMANCE OR COMPLEX ACFT & NO ENDORSEMENT TO OPERATE SUCH ACFT WAS FND.
Source: NTSB Aviation Accident Database
Aviation Accidents App
In-Depth Access to Aviation Accident Reports