Aviation Accident Summaries

Aviation Accident Summary BFO87FA027

EDGEWOOD, MD, USA

Aircraft #1

N112BB

Rockwell 112

Analysis

ON THE DAY OF THE ACCIDENT AND BEFORE THE ACCIDENT FLIGHT, THE INLET FUEL HOSE TO THE FUEL FLOW DIVIDER WAS REPLACED. THE HOSE ASSEMBLY WAS FABRICATED BY MAINT PERSONNEL. AN INSPECTION FLIGHT AFTERWARDS REVEALED ENGINE ROUGHNESS DURING FUEL MIXTURE LEANING. AFTER THE INSPECTION FLIGHT, IT WAS CONCLUDED THAT FUEL FLOW WAS INADEQUATE AND THE FUEL INJECTOR NOZZLES WERE CLEANED. A SECOND INSPECTION FLIGHT REVEALED SATISFACTORY OPERATION DURING FUEL MIXTURE LEANING AND THE ACFT WAS RETURNED TO SERVICE. ENGINE POWER LOSS OCCURRED SHORTLY AFTER TKOF WHEN THE ACFT WAS CLIMBING TO CRUISE ALTITUDE. A LOSS OF CONTROL OCCURRED ON THE ACDT FLT, AS THE PLT WAS ATTEMPTING A LANDING IN AN OPEN AREA ALONGSIDE RR TRACKS. THE ACFT ERUPTED IN FIRE AFTER GROUND IMPACT. EXAMINATION OF THE ACFT REVEALED PIECES OF RUBBER INSIDE THE FUEL FLOW DIVIDER.

 

Source: NTSB Aviation Accident Database

Get all the details on your iPhone or iPad with:

Aviation Accidents App

In-Depth Access to Aviation Accident Reports